I Bought a Cheap Porsche 996 Turbo and It's Unfixable

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  • Опубликовано: 11 июн 2023
  • Fook this car!! I've at my wits end with the 911 Turbo! I've never been so stumped and frustrated with a vehicle in my life.
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Комментарии • 419

  • @tbasmwmc
    @tbasmwmc Год назад +136

    There's no shame in having a pro take a look at it.

    • @qc7767
      @qc7767 Год назад +2

      My thoughts too

    • @bubberrand
      @bubberrand Год назад +2

      That’s what I would do. Matt has given it his all.

    • @palikariena7292
      @palikariena7292 Год назад +2

      There’s no fun in that.

    • @IM_8685
      @IM_8685 Год назад +2

      ​@@palikariena7292 well the thing is it is obviously something that is unaffected at atm pressure but opens up at little bit of pressure

    • @vettesrule3170
      @vettesrule3170 Год назад +1

      @@palikariena7292 You call what he's going through "fun"?? Sadist, so maybe YOU can fix it for him and achieve a higher level as a masochist...You know, for the FUN of it.

  • @gibby3820
    @gibby3820 Год назад +105

    I would cut your losses and drop the engine instead of fighting that tight bay week after week 🤷‍♂

    • @marvinvisser5039
      @marvinvisser5039 Год назад

      My thoughts exactly

    • @zascar
      @zascar Год назад

      Maybe this was his plan all along - I mean it's great content! :))

    • @matt13ross
      @matt13ross  Год назад +2

      I'm really trying to avoid that because it's going to be a dive into the rabbit hole. I just want to enjoy it stock ish for a while!

  • @vvelazquez79
    @vvelazquez79 Год назад +82

    Might be easier to just drop the engine to pressure test it again. You'll definitely be able to see exactly where the smoke is leaking from that way.
    Still pulling for you to get it fixed!

    • @cvpuga
      @cvpuga Год назад +1

      agreed

  • @nev997TT
    @nev997TT Год назад +48

    Boost leak aside, the larger throttle body and plenum may require the car to be tuned. Might be worth talking to one of the tuning shops in your area just to get their take on it as it could be resulting in the high idle. Not sure where in Maryland you are, but RPR Automotive and TPC Racing are the shops with which I’m familiar.

    • @olivervaldes4223
      @olivervaldes4223 Год назад +2

      This comment right here is the answer. A second set of eyes would be nice and you get to support the local community.

    • @matt13ross
      @matt13ross  Год назад +3

      I will eventually get a tune, but the goal is having it running / driving correctly in it's stock ish form first.

    • @sunnohh
      @sunnohh Год назад

      @@matt13ross might not be possible with physically different parts though, like to avoid the tune you need stock parts most likely, might be easier to just get a tune

    • @zav8687
      @zav8687 Год назад

      Rpm in Hagerstown is cool too

  • @OZBIE
    @OZBIE Год назад +20

    Check the wastegate actuator as mentioned below, they have a tendency to stick.

  • @zascar
    @zascar Год назад +6

    Dude we are all here with you - Keep at it!! As others have said no shame in getting a pro to help diagnose. Dropping the engine would be a great set of videos for sure! And the relief and celebration we'll all have when you finally fix this thing will be amazing!

  • @Harvy500
    @Harvy500 Год назад +19

    Don't give up!!
    It's been a long journey and don't stop when you're so close to the end.
    I'd suggest & I know it's a lot of work, but drop the engine. Hook it up as close as possible if it was in the car then you can and smoke test it again.
    Good luck from Sunny England!!

    • @matt13ross
      @matt13ross  Год назад +1

      Trying to avoid an enjoy drop for now.

  • @dailydriven991
    @dailydriven991 Год назад +4

    I suspect the idle is a separate issue from the boost leak. You were hitting .6 bar and not even at redline so it was still climbing. Keep in mind these cars need to rev high. Mostly I think it would really benefit from a good tune. Especially with the new throttle body and putting the stock air box back in. Who knows what the previous owners did with it.
    P.S. another vote for dropping the motor if you’re going to keep chasing the boost leak. If you do that, might as well change the plugs/coils while you have it out and clean the map/maf sensors. That should smooth her out quite a bit.

  • @CRE8TEDbyGod
    @CRE8TEDbyGod Год назад +1

    My hope is that you find the fixes needed. I have really enjoyed the journey and really love watching all the videos. Thanks for taking the time to take us all along. :)

  • @B0RRAC0
    @B0RRAC0 Год назад +2

    This channel reminds me of the Chris Sullivan channel. Just a guy in his garage wrenching on his car! Love it!!! 😁👍🏼

  • @BG-ri8ww
    @BG-ri8ww Год назад +2

    I’ll echo the crowd.
    You’ve put massive work into this. Well done, don’t give up.
    The old saying “you can’t see the wood for the trees” is valuable.
    A second set of eyes might cost a few bucks, but their experience might just say. “Hey all you needed to do was…..”
    Once it’s running all the frustration will quickly pass.
    Keep at it. We’re behind you on this. 😊

  • @Airliner1964
    @Airliner1964 Год назад +6

    Matt, love your content and the awesome editing you do for your videos. Always looking forward to your next one! This 996TT was a hot mess when you got it, but now she's a definite looker. Don't give up on making it exactly how you want it. You are truly gifted in the work you do on these speed machines, but maybe it's time to have a Porsche Tech have a look at it? Either way, good luck.

  • @YogisGarage
    @YogisGarage Год назад

    I have the same smoke machine. Love it. Gonna check out those cup holders. Now that i'm driving my two 911's I need something to hold my stuff! Did you forget that you have a positive post in the engine bay so you can run your smoker there? I did... once. 13:01 Did I just see the tripod on your gimbal go up down by itself? The computer should tell you have a massive vacuum leak. It may not throw a code right away.

  • @Weidjeep
    @Weidjeep Год назад +12

    Do not give up, this car has come a long way under your ownership. Take a break and turbo the E36 lol, and try to find a Porsche "shop" that will work with you to find the issues and see if it just needs a tune? Either way many people in the chat would be sad to not see this car 100% again. But you gotta do what you think is the best viable option for success. Great work and we are all excited to see what your next steps will be.

    • @matt13ross
      @matt13ross  Год назад +2

      No turbos on the E36! That car is simple and works well lol.

  • @TheSwampDonkey
    @TheSwampDonkey Год назад +2

    First thought, maybe try to put the stock throttle body and plenum back on, is that an option? If the car idles correctly with those being stock, as another poster said, possible a tune is needed to correct the airflow. However, the idle being high def makes me think of a vac leak somewhere. Have you tried an E-Gas reset? What about unplugging the MAF to see if anything changes? A bad MAF will throw off the airflow readings. If you unplug the MAF and it idles normal, you have a bad MAF. Also, check the oil cap and oil filler tube to see if they are cracked. Hope you are able to get it fixed.

    • @matt13ross
      @matt13ross  Год назад

      Nah the stock plenum broke. E gas reset? Unplugged the maf and it barely ran lol.

  • @S2NAZ
    @S2NAZ Год назад +5

    Well, I’ve seen this many times in my early years where owners try to make repairs, then take that walk of shame to a repair shop. I applaud you for your tenacity, don’t give up. You can try closing the throttle body butterfly to force the engine to draw more air through the leak, then take a small hose to your ear and start listening more accurately for the source of the leak. You can also try shooting a little starting fluid around the area you suspect might be leaking and see if the idle rises, that might help you narrow it down. Good Luck Matt!!

    • @matt13ross
      @matt13ross  Год назад +1

      I've tried the starting fluid, didn't change the idle, which was weird. I'm going to try a hose to my ear.

    • @S2NAZ
      @S2NAZ Год назад +1

      @@matt13ross I used to use a stethoscope probe with a longer hose attached to the end. Worked really well.

  • @BleezyD
    @BleezyD Год назад +3

    You got this, Matt!!! Were all pulling for ya.

  • @IanClos3
    @IanClos3 Год назад +1

    You've done so much by yourself and the car has been brought back from crap to outstanding! Can't beat yourself up as the computer systems in porsches are finicky as I am learned myself on my 02 996. I purposely avoid stock turbo setups because of the issues and I am not yet at that stage to learn about them myself. BUT, I would say it couldn't hurt, nor do I think would anyone hold it against you if you took it to a local specialist, not a dealer obviously, to see what you may have missed. Sometimes they have the expensive tool that can connect to the obd2 and read everything and every sensor and will lead to a faster diagnostic or they may just have seen this before. That would be my suggestion if you'd like to reward yourself and take a break but also solve the issue so you can enjoy the car. Good Luck man! As always I love the content, love my poorsche shirt, and hope you get it figured out!

  • @jorgebaqs7370
    @jorgebaqs7370 Год назад +1

    just subscribed, I know that feeling brother Porsches can be tricky. Do not give up!

  • @JT-162
    @JT-162 Год назад +22

    Your being frustrated and figuring it out is why I watch! Hang in there and don't give up.

    • @moneymikeslickwill8749
      @moneymikeslickwill8749 Год назад +5

      100% agree matt we rooting 4 u bro

    • @Badmudaphucka
      @Badmudaphucka Год назад +1

      Great car for the channel, but terrible for the hosts mental health it seems?

    • @matt13ross
      @matt13ross  Год назад

      Thanks guys!

    • @Crime_pays
      @Crime_pays Год назад

      You’re a sadist and an Machiavelli

  • @myd00m
    @myd00m Год назад +1

    Very good video, that cup holder is very similar to the one in my BMW 1 Series coupe.

  • @robwilson7897
    @robwilson7897 Год назад +3

    I had a similar issue. Mine turned out the be the left side lower boot between the left intake manifold and the tube that connect to the right manifold. The hose band is tight but it slipped off the back where you cant see it. It will require some stretching and acrobatics to get to it. I watch your videos but dont read the comments. I have 2 996tt both I dropped the engines to do the coolant pipe pinning and replace aging rubber hoses. I highly recommend it. It not as hard as most people say. the only special tool I used was a lift table.

  • @Ali-xg2cc
    @Ali-xg2cc Год назад +4

    I Love this channel because damn bro it's so relatable!! If anyone is a car guy, you know the feels 🤣You'll figure it out bro, keep pushing

  • @joncamilleri2172
    @joncamilleri2172 Год назад +1

    Keep at it, you are so close. Agree with other comments that there is no shame in getting a pro to take a look at it.

  • @MrRedkid91
    @MrRedkid91 Год назад +3

    check the charge pipe/hoses from the turbos to the the intercoolers. I've had them pop off and my idle was having similar behavior

  • @Berti_00
    @Berti_00 Год назад +1

    Every time a video gets dropped, i get excited. You got this, bro

  • @keithvolner930
    @keithvolner930 Год назад +3

    I feel like you and markski should team up on this one! Common Deejay, help this brother out!

  • @cliffkemp201
    @cliffkemp201 Год назад +1

    Having as much fun as I am. I bought mine in 2018, upgraded a lot of stuff, even spent a decent amount on rebuilding the transmission (manual). Been in the shop ,mostly, since 2021. Had the upgraded stuff done late 2020. In the shop now. Put about 3k miles on it since 2021. The shop is still sorting it out and, we think it is possessed.... lol. 04 convertible.

  • @slic1one
    @slic1one Год назад +4

    I once had issues with idle keeping at 2k rpm and even going up by itself just due to a faulty new (!) MAF sensor. I would assume you'll need to run an adaptation or something for the TB, VAG cars are known to be very particular about the airflow

  • @gouldnj
    @gouldnj Год назад +4

    You’re doing this right Matt, but WHERE you introduce the smoke is the important part when chasing boost leaks. It could be on the hot side, cold side, recirc/blow off. You need to be methodical and use diagrams of the systems. Good luck. PS-Have you gotten the tow hook plug installed in the front bumper yet?!

  • @plus790
    @plus790 Год назад +7

    The yellow console is great and that Etsy guy seems to make good quality 3D printed stuff--that cup holder is outstanding! Not a fan of the parking brake condom though. For the leak, use a borescope camera to get back in there!

  • @zachbitzer8467
    @zachbitzer8467 Год назад +1

    Not sure how these are setup, but back in the b5 s4 days when we used to pressure test them, we had to make sure any pcv hose off the intake/ypipe was also plugged. If not, the air is just going to escape into the crankcase. It should be able to hold the pressure you feed it and slowly bleed off.

  • @mythos000000025
    @mythos000000025 Год назад +1

    Wish I could afford it..still gotta put together my fd3s project...keep it up man, the car looks nice (not a yellow fan personally but it does look good)...you'll find its probably something small along with a new tune. Turbo cars(especially German ones) require programming for EVERYTHING...I've got an F30 awd bmw...yeah you change something you gotta reprogram. Somethings are fine if your not changing anything mechanical other than say exhaust or charge pipes....but bigger bov....depending like to atmosphere, tune, bigger throttlebody, tune, bigger injectors, tune, etc, etc

  • @charha01
    @charha01 Год назад +1

    At some point you may need to drop the motor. I've never done it, but I've talked to several people that have an they all say it's not bad since these cars are designed to be race cars, and so pulling the engine is something that is planned and designed for. Once you have it out, you can fully see everything and I'm betting you have some hose or connection cracked or broken that you just can't see with the engine in. It would also be a perfect time to do the AOS replacement and maybe even the coolant tank as those are PITA to do with the engine in. Good luck man... I feel your pain.

  • @jouleskelvin
    @jouleskelvin Год назад +4

    Don't get discouraged. It's an amazing car and you've really brought it back. We're learning with you, too. So, take a break and go back to it next week. We'll be watching. 👍🏁

  • @momchilmestchiev1583
    @momchilmestchiev1583 Год назад +4

    It’s a bmw x1 cupholder it’s the same mount and positions in my mom’s x1 there is even a spot in the armrest cubby to store it

  • @aslee143
    @aslee143 Год назад +1

    Watching this a few days after upload, and from reading the comments, here are some ideas you can try before dropping the engine. 1. In my experiences with turbo cars, the blow off valve/by pass valve/waste gate seems to be a big issue when it comes to boost leaks. 2. Trash tune. See if you can retune to stock tune. 3. Maybe new maf?

  • @KemDIY
    @KemDIY Год назад +1

    Your tenacity in problem solving is truly inspiring.

  • @WayApp
    @WayApp Год назад +1

    Wishing you all the best in finding creative solutions and turning it into a remarkable ride! 🏎✨

  • @chrisg2779
    @chrisg2779 Год назад +1

    I have a habit of forgetting how things go back together. Which is why I always take pictures of those thingamajigs before I take them apart.
    Saves me lots of time.

  • @Smellyal8r
    @Smellyal8r Год назад +1

    That cup holder is from a 1 series bmw or z4. It’s weird shape is meant to hold a standard coffee mug with a handle.

  • @e1kaiser482
    @e1kaiser482 Год назад +1

    Have you consider that the boost pressure sensor is bad. also could be that these recirculation valves are broken. best at this point i think that is drop the engine and replace every gasket and oring, and yeah there check the sensor and valves
    Its pretty amazing how this car still fight you this hard. i hope so much that finally runs well again

  • @oasisalek
    @oasisalek Год назад +2

    I have noticed you have tilted your motor down by taking out the rear mounts a couple of times to give you better access. I have a feeling by doing that you might have hairline cracked the plastic manifold on the front left side of the motor right along the firewall. There are long plastic mounts on it and they can crack at the base if you tilt the motor down without unbolting the stuff mounted to it. Worth a look, this happen to me years ago and was very hard to find, I pressure tested and smoked…. The smoke only came out when the engine was under load, that’s when the crack opened up bigger…. My idle was at between 2500 and 3000 rpm. Hope this helps!
    Mike Salek

  • @adambrand1305
    @adambrand1305 Год назад +2

    The plastic intake runner on the drivers side is also known to rub through / crack and create a leak.

  • @carlodomingo5504
    @carlodomingo5504 Год назад +1

    God bless you for not cussing out a storm. At least not on video. I would be! I usually have no interest in watching a video that is not related to my non turbo 996 but your video editing and pleasant demeanor makes me keep coming back!

    • @matt13ross
      @matt13ross  Год назад

      Awesome to hear thanks! And trust me I curse behind the scenes plenty lol.

  • @craftingmat5425
    @craftingmat5425 Год назад +2

    No, Mat! Dont give up!
    I think this car has not seen a major service for 10 years... main reason most likely.
    But secondly: You have a larger trhottle installed -> I think that thing needs an urgent setup and remap.
    Also would not drive too far and too hard with it as is - it may run lean?
    Go for a setup and remap.

  • @thesearch9048
    @thesearch9048 Год назад +1

    Add me as another suggesting to drop the engine to get it all figured out. You are close to getting it all sorted out! Looking forward to the next vid!

  • @MrFunnyDad2024
    @MrFunnyDad2024 Год назад +1

    Fought an old 911E w/ Mech. Fuel Injection, became a exercise in SM. LOL. But country repair job - always works. Accidentally drop some matches. Southern Lighting... LOL

  • @themuz3
    @themuz3 Год назад +1

    I called IPD when i couldn't get my plenum to fit (the crossmember was 180 backward from factory). They told me the larger throttle bodies don't run as well for daily use.

  • @aa240sx
    @aa240sx Год назад +7

    don't give up. you put time and money into it. from all accounts, this is still repairable and it's not engine internals. you can do this!

  • @challengerjetdriver
    @challengerjetdriver Год назад +1

    Sticky waste gate lubricate with mouse milk, yeah that’s how we call it. Keep the faith you are getting there 💪

  • @Euuuhhhful
    @Euuuhhhful Год назад +1

    These cupholders have been used in bmw x1 (an probably other lines) from 2010 onwards

  • @Tetriiix
    @Tetriiix Год назад +2

    Matt! There is nothing bad to reach an “expert” on the matter!! You have done way more than me on my car!! Next step is basically dropping the engine!!

  • @miketurco5282
    @miketurco5282 Год назад +1

    Keep your head up Matt many of us have been there. A break will do you good.

  • @paulpalmer8235
    @paulpalmer8235 Год назад +1

    It hit 0.6 Bar so only down abit - the upgraded parts might be needing tuning to make the most of them which might be causing the .2/.1 of boost loss?!
    Love your content - one of the best watchable build channels out there
    Well done Matt 😊 👍👏

  • @fd3s7
    @fd3s7 Год назад +1

    OK, the big thing to think about with a high idle is air. The throttle body restricts air going to the engine. If the engine gets NO air, it would not run and would stall. If you give it just the right amount of air that will set the idle speed. Too much air and the idle will be too high. If you have a larger than stock throttle body and the ECU commands it to open a certain percentage, that may be letting more air in and setting that higher idle. Other possibility is a vacuum hose that is connected after the throttle body (between TB and engine) that has a check valve or something like that that is failed or backwards and letting more air in than should be getting there.

    • @fd3s7
      @fd3s7 Год назад +1

      Also don't give up! You are SO CLOSE! Analyze the situation, do testing, get evidence, move forward. You can do it!

  • @MrRedkid91
    @MrRedkid91 Год назад +1

    also check the wastegates on the turbos maybe possible that its broken or stuck

  • @Badmudaphucka
    @Badmudaphucka Год назад +1

    Pull off the pipes, hoses & plenum, etc, block the ports & test if they hold pressure on the bench (either with smoke or in a tote of water) to rule them out one by one. If there’s anything you can’t access as part of the intake / vacuum system I’d assume it’s all to blame & replace it in one hit with a motor drop. Have you looked at the turbo’s? Checked the waste gates are staying shut while boosting? (Just pull them off & send them away for a refresh with billet wheels & drop the motor so you can see what you’re dealing with on the leak & fix whatever other goodies you find).

  • @lukeharrielson9357
    @lukeharrielson9357 Год назад +1

    Dude I’m so frustrated for you 🤦🏼‍♂️ but your so close! The car is looking so freaking good! Maybe just take break for a while and come back!! We believe in you!!💪🏼

  • @shr00m7
    @shr00m7 Год назад +5

    YOU'RE SO CLOSE! And selfishly, I need to know what the problem is. I know this might go against the ethos of your channel, but have you thought about taking it to a dealer or independent Porsche shop just to get a diagnosis? It may be quicker and a good learning experience, especially if you can find a shop that will walk you through the diagnosis (maybe in exchange for some free internet publicity)? Then you can just fix it yourself in your garage. Anyways, I am pulling for you and the Porsche!

    • @Badmudaphucka
      @Badmudaphucka Год назад

      Or get it diagnosed & then just pretend like you found it yourself when you shoot the video & fix it.

    • @matt13ross
      @matt13ross  Год назад +1

      I may have a shop diagnose, but I'd like to do the fix. The diagnosing is killing me!

  • @dariencrawley8841
    @dariencrawley8841 Год назад +1

    Im from Maryland as well would love to show you my SLK when its done

  • @seatschris
    @seatschris Год назад +2

    Dropping motor would be easier to work on trust me on that one,as mentioned below already check wastegate actuator and car might need tuning and bolt ons may be past Ecu self learning capacity. If you do really sell the car I’d be interested 😊

  • @jonathanownsyou
    @jonathanownsyou Год назад +1

    That cup holder I'm almost certainly sure is from a mid 2000's BMW 6 series. My Dad had a 645Ci and it had that cup holder. Not sure if it was used in anything else.

  • @thepacketnarc7634
    @thepacketnarc7634 Год назад +4

    Hey Matt. You know there’s a few rigid vacuum lines back behind the plenum and running near the left and right sleeves ? Make very sure you haven’t cracked or broken off any of those rigid lines. They are fragile like Pocky sticks.

  • @cycoracing
    @cycoracing Год назад +1

    Looking at the last shot of the engine bay in the video, I think you have the diverter valves in backwards. As well high idle is usually caused by a vacuum/air leak. Google 996 turbo diverter valve installation and try a throttle body adaptation/reset.

    • @matt13ross
      @matt13ross  Год назад +1

      Yup, I've got those flipped around now.

  • @pietervanommen
    @pietervanommen Год назад +4

    engine out seems to be only way to figure out

  • @OhYeahAboutThat
    @OhYeahAboutThat Год назад +9

    That cup holder is awesome, but it's $169.00 before discount and still $152.10 after. That's a pretty steep price that may turn off a lot of people.

    • @jmqwert
      @jmqwert Год назад +1

      Hmm when owning a porche 911?

    • @Jagman2919
      @Jagman2919 Год назад +1

      You can afford owning a Porsche 😂

    • @MrEggomylego
      @MrEggomylego Год назад +1

      That's Porsche tax for ya

    • @ideabrickworks9043
      @ideabrickworks9043 Год назад +3

      I just got the cubby, and the quality is excellent. I have found hat you get what you pay for with 3D printing. I will be ordering mine soon!

    • @matt13ross
      @matt13ross  Год назад +2

      Meh, I don't think the price is bad at all. It's a GREAT design and fitment is outstanding.

  • @bernardthefourth
    @bernardthefourth Год назад +1

    You need a durametric to do some logs and see what's going on. I'd hire Markski to read the logs and get some advice.

  • @jaimermb
    @jaimermb Год назад +1

    By this time i would drop the engine a check everything. working in that little window of trunk it´s bad!

  • @dubzstylerc9580
    @dubzstylerc9580 Год назад +1

    Okay, so it could be one of two things maybe the idle control valve unit is faulty , but then, saying that you would get a correlation code, for that, or it may be a case of doing a complete relearn for all of the systems, so it’s all reset to 0, especially the throttle body, now I’m pretty sure you have got the equipment to reset the throttle body values. I know on VW‘s you can do a manual reset by just put in your foot on the throttle when the car is turned off., still keeping your foot on the throttle. Turn the car on but do not start hold for 10 seconds, then release the throttle completely take your foot off of it and then turn the car off.

    • @matt13ross
      @matt13ross  Год назад +1

      Solid suggestions, I tried a few of them, thanks!

  • @millertimebmw
    @millertimebmw Год назад +1

    Keep the content coming!

  • @cmorse508
    @cmorse508 Год назад +1

    would it be worth blocking the intake tubes at the Y pipe going into the intake? is there a chance that its just bleeding into the motor and not holding pressure. that way you are checking all of the tubing before the motor.

    • @matt13ross
      @matt13ross  Год назад

      I can hear is escaping somewhere.

  • @brandonmulford5524
    @brandonmulford5524 Год назад +1

    Time to sponsor an Indy Porsche Mechanic who wouldn't mind working for a discount. Hell, try linking up with Omega Auto and the Car Wizard that would be worth a few views for sure!

  • @PompeyMatt17
    @PompeyMatt17 Год назад +1

    24:08 I went "whoa!".. as in Europe, well.. UK.. black pumps are diesel 😀

  • @craigsmith1354
    @craigsmith1354 Год назад +1

    You are seeing your idle high .it could be an internal air leak behind the throttle .this could be caused by engine breather . It could also be the plenum that you installed. I'm not sure if you did a throttle body adaption to reset it . Reach out to Ross tech vcds to go through the readiness settings to verify your repairs .Audis porches vws and all their cars have this capability try it out . I feel your pain though 😢.

  • @petesmith3306
    @petesmith3306 Год назад +1

    Stick with it Matt. Youre very close now. Personally, Id double check that the throttle body and inlet manifold bolts are the right length and and are properly torqued down and have it properly set up by a pro then enjoy the car. You've done everything right so far and deserve to enjoy it over the summer. The car seems like a perfect candidate to have a dodgy 'tune' from a previous owner. If youre not sure of its history, thats another good reason to get it properly set up by somebody who knows what they're doing

    • @matt13ross
      @matt13ross  Год назад

      No tune on the car. When I bought it, it was at .7 bar all the time with intake and exhaust.

    • @petesmith3306
      @petesmith3306 Год назад +1

      Thats probably good news for you, Matt. Good luck with it all.

  • @jamesp5624
    @jamesp5624 Год назад +1

    Ok, not sure if it’s been said, but:
    1) do a throttle position reset. Look up the procedure, it’s simple.
    2) get an odb redder with an app that will show you the throttle position in real time.
    3) Re-check the n75 valve and its connections
    4) leave the battery unplugged overnight to reset the DME.

    • @jamesp5624
      @jamesp5624 Год назад +1

      Honestly, I think you fixed the boost leak if it held air that long. You’re now fighting with throttle/DME/tune issues I think. Maybe going into limp mode without a code thrown.

    • @matt13ross
      @matt13ross  Год назад

      Awesome tips thanks!

  • @danielduchon1035
    @danielduchon1035 Год назад +1

    Keep it up! 🖖🤜

  • @mike-mx7ic
    @mike-mx7ic 6 месяцев назад

    Isn't boost leaking though the throttle body into the engine?

  • @Petrol_fix
    @Petrol_fix Год назад +1

    Could be one of the intake boots under the throttle body

  • @Jagman2919
    @Jagman2919 Год назад +1

    Drop the engine……
    Smoke test that way
    You got this man!

  • @reloop7691
    @reloop7691 Год назад +1

    you should get 0.7 bar at around 6000rpm when it's producing max power. I get max boost at around that in my 996 turbo S.

    • @matt13ross
      @matt13ross  Год назад

      I think it should come on sooner than that.

  • @danielsplayhouse3804
    @danielsplayhouse3804 Год назад +1

    If it has an idle control valve on the throttle body check it first!!

  • @AaronBesson
    @AaronBesson Год назад +1

    You maybe should have done the smoke test with the throttle body off. You would have eliminated that and also had more room. Also you need to get the car tuned for the plenum and other mods. Hate to say it. But a visit to a Porsche mechanic shop for a 250-500 buck inspection could have quickly diagnosed everything and saved you lots of time fixing it yourself.

  • @BrandonErina1972
    @BrandonErina1972 Год назад +5

    I would suggest taking the engine all the way and fix any trouble areas and anything that could be updated for the future. That way you fix everything when it’s out

  • @milanulrich
    @milanulrich Год назад +8

    not sure if you changed the throttle body, as I haven't seen all the episodes, but if you did that, it means the more air is able to get in even on the 1° (closed valve) position and car is trying to compensate with more fuel to get the gas/air right. Thus higher idle rpm and lower boost as well. Did you tried original throttle body?

    • @janichols13
      @janichols13 Год назад +1

      I agree that this is a good place to start. Might also want to do a throttle body adaptation to help make sure it's actually getting true readings. Also be good to hook a scanner up and check the fuel trims. Although it probably needs another couple of drives to adapt.

    • @matt13ross
      @matt13ross  Год назад +1

      Throttle body re learn is on the list!

  • @andrew_barros
    @andrew_barros Год назад

    Have you scanned for fault codes that don't pop up as CEL? Sometimes you just need to clear the codes, start the car, turn off key out and back on again for it to relearn.

  • @mirzahamza6017
    @mirzahamza6017 Год назад

    You blowing on that pipe your subscription just went up by 150000😂❤

  • @nickmitton7350
    @nickmitton7350 Год назад

    Have you got a code reader/ scanner to check the measurements on all the systems? If not a rolling road for tune with the new throttle body might be the way to go. ? 🤔🤔

  • @ClioSport2016v
    @ClioSport2016v Год назад +3

    Holder is from BMW

  • @scotts2k
    @scotts2k Год назад

    Why didn't you smoke test from throttle body as you reassembled it. Also, if you went larger throttle body, don't you need a flash to compensate for additional air at idle, hence high idle. Also, did you do the reprogram of TB after reconnecting the battery? Turn on ignition for at least 1 min, then off for 10 plus seconds, then start?

    • @matt13ross
      @matt13ross  Год назад

      I don't think I need a tune. Reprogram is a solid idea though!

  • @alexcaragea6049
    @alexcaragea6049 Год назад +2

    Cmon man. Cracked head, injector seals, head gasket, tb gasket, waste gates leak, turbo leak, crankcase ventilation leak

  • @subes5873
    @subes5873 Год назад

    Wouldn't the air escape out of the exhaust??
    I mean one or of the pistons will be down no?

  • @user-rj2le6hj3m
    @user-rj2le6hj3m Год назад +2

    Matt try giving Sam at BY Design a call. He is a good guy and may be able to help you. He has done hundreds of these 911 turbos and a bigger supporter of the community.

  • @BMW2002M10
    @BMW2002M10 Год назад

    Cupholder looks like one from BMW, specifically the e63/64 gen 6 series

  • @MrJbipes
    @MrJbipes Год назад +2

    I have an '05 Boxster, 987. The layout is somewhat similar on the top of the engine. I had replaced my starter, which is on top of the engine. I had to remove the plenums that fed the intakes. Loosened the large diameter hose clamps each side. (same as your car) to remove the plenum. After buttoning it all up, a week later I got very rough starts when cold. This went on for a few months, tried everything. It turned out, one of the hose clamps was askew on the bottom, where I could not see it, giving a small vacuum leak. Another Porsche 996 guy told me to check it with a mirror under the plenum. Sure enuf, that was the problem. The off-kilter hose clamp on the edge of the rubber boot was just enough to open it for a leak. It's been working great now for 3 months. Hope this helps. look here: ruclips.net/video/MN206c5W1T0/видео.html

  • @bcut
    @bcut Год назад +1

    take a break from it come back with a fresh mind and some patience built back up. 😎theres no hurry right? we'll be here for you! :) 👍👏👏👏👏

  • @natetrombley9488
    @natetrombley9488 Год назад +1

    I would put money that you need a throttle body adaptation. I've never seen a VAG car that can relearn a throttle body. When I upgraded my s5 throttle body I needed use the adaptation software from my tuner so the car would know what's going on.

  • @TheBullockFamily
    @TheBullockFamily Год назад

    Can you try mounting a GO Pro with light back where you can’t see then add smoke and air and see if the Go-Pro can capture the smoke

  • @Alex.P_10
    @Alex.P_10 Год назад +1

    This high idle leads me to think it's a crankcase ventilation issue 🤔