NS 15R Rips End Of Hopper Car Off And Goes Into Emergency Leaving Chester SC

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  • Опубликовано: 27 сен 2024
  • As I was filming NS Train 15R departing Chester SC on the NS R Line heard the train go into emergency and got the footage as the train came off the track.

Комментарии • 87

  • @crollwtide9452
    @crollwtide9452 Год назад +38

    One of those old rusty hoppers must have disintegrated under the pulling stress it was under...that was an interesting catch for railfanning.

    • @rxrcond4life
      @rxrcond4life Год назад +2

      Engineer was pretty heavy into dynamic brake in video. Not pulling...

    • @MilwaukeeF40C
      @MilwaukeeF40C Год назад +4

      Hoppers get corrosion problems, especially from stuff like fertilizers.

    • @crollwtide9452
      @crollwtide9452 Год назад +1

      @MilwaukeeF40C J could expect that from all the years of usage they would get

    • @BRIANumber7-RCandModels
      @BRIANumber7-RCandModels 11 месяцев назад +1

      It was definitely pulling with the sound of those GEs chugging like that.
      I've heard an EMD start whining just like that as well on and off while going up a grade. Why it does it intermittently? I'm not sure (maybe it's the cooling system), but it was definitely going uphill since I was at an area where the 7,000ft train's front and back end were about 300ft from each other after it rounded a horseshoe curve on the mountain grade it was climbing.
      What is interesting to me, is it broke with only three engines pulling it with no changes in slack action. Usually knuckles start breaking with four engines without any slack action happening. That hopper must have been really rusted out.

    • @paulblichmann2791
      @paulblichmann2791 11 месяцев назад +2

      Ive seen hoppers still painted "Milwaukee Road" at crossings. There are hoppers out there older than dirt.

  • @ShamuXEagleDriver
    @ShamuXEagleDriver Год назад +35

    Chris, did you put a penny on the track, . . . again? 🙂

  • @benchedthatpiece
    @benchedthatpiece Год назад +23

    Not something you see every day, nice job on this!

  • @milepost26.69
    @milepost26.69 Год назад +10

    I chased this exact train out of Rock Hill but ended up not getting ahead of it. Too late to get it into Chester. Neat catch though

  • @thomabb
    @thomabb Год назад +10

    You didn't get any additional footage of the carnage? A closer shot of the hopper?

    • @kishascape
      @kishascape 11 месяцев назад +3

      Barely even got a shot of the hopper. Failureeeeeeee

  • @NorthernOhioRailroadAction
    @NorthernOhioRailroadAction 10 месяцев назад +1

    Excellent video really enjoyed it keep up the great work thanks again and have a wonderful safe day

  • @ColumbiaAreaRailProductions
    @ColumbiaAreaRailProductions Год назад +8

    Yeah, that'll buff itself out.....

    • @LivingWRailfan
      @LivingWRailfan 7 месяцев назад

      Everything does
      Just like CP 7011 was buffed rigth out

  • @johnandrus3901
    @johnandrus3901 Год назад +8

    He 'lunged' it. Just pulled the end of the car right out. I'm surprised that the truck went with it. Wasn't slack action, he was pulling at the time. Probably an unnoticed defect of some sort.

    • @BenjaminEsposti
      @BenjaminEsposti Год назад +6

      Possibly the car was already damaged (cracked weld/plates) and just failed.
      Years back there was an incident where a tank car split in half due to a bad weld. Dumped acid everywhere. Pretty crazy.

    • @mshum538
      @mshum538 Год назад +2

      Lots of these defects are often found when a train is “ made up “ and the car inspectors walk the track coupling the hoses and inspecting each car, car inspectors know what to look for and PSR has to go…..

    • @rc391995
      @rc391995 Год назад +4

      He didn't lunge nothing and he wasn't pulling . he was running dynamic brake . bad order car center pin failure .

    • @BlackMan614
      @BlackMan614 11 месяцев назад +1

      @@mshum538 Yeah… and the train master tells them to send it anyways. Happens every day. Especially NS… but not exclusive.

    • @Joe-d7m6k
      @Joe-d7m6k 4 месяца назад +1

      ​@@mshum538What car inspectors, at NS????????

  • @lukebakerlpb9034
    @lukebakerlpb9034 5 месяцев назад +3

    Dammit Bobby 😂😮

  • @Johnny64ism
    @Johnny64ism 11 месяцев назад +3

    Great Catch but would have loved to have seen the damage 2 the hopper car you cut the video way to short

  • @grandcrappy
    @grandcrappy Год назад +4

    The carriers task us with long, ugly trains but are in our business if there are problems.

  • @JointedStudios
    @JointedStudios Год назад +8

    I heard the leading locomotives go into notch 8, which could mean that they pulled too hard, causing the train to slack and shove the lead truck of the hopper out.

    • @rxrcond4life
      @rxrcond4life Год назад +3

      Those are computerized units. You can go from stop to run 8 and the computer only allows a certain amount of load. More likely stretched the train in undulating territory. Poor train handling...

    • @rc391995
      @rc391995 Год назад +4

      I don't know what you think you heard but he didn't go from dynamic to a number 8 power position I can hear as well . I don't know the terrain but he was leaning hard on the dynamic when he crossed the crossing and continued to do so till it come into . bad train handling that's possible but I highly doubt it. My guess is bad maintenance and the hopper was pushed off the center pin .

    • @haroldreardon1407
      @haroldreardon1407 11 месяцев назад

      Comment of 8th notch made no sense as they were in dynamic at the time. Could have been stated better.

    • @elfnetdesigns702
      @elfnetdesigns702 10 месяцев назад +2

      First off those GE's are MU'ed so if the lead (master) goes run 8 so do the slave units, Next those locomotives are MCU controlled or computer controlled and monitored, this means they have coded parameters that set load limits based on different conditions, You can go in to run 8 but the computer may not allow the engine to increase RPM or allow the generated power to be delivered to the traction motors, this is all efficiency, safety and failsafe systems.
      The likely cause is neglected car inspection and maintenance, and the cars age sand condition does not do any favors. I would have to say that the care was just worn out, old and tired so it gave up

    • @master7chief
      @master7chief 10 месяцев назад

      They were definitely pulling and reached for notch 8 as the SD70ACC cleared the crossing. Maybe some are thinking dynamic braking because the EMD's radiator fan sounds just like an EMD dynamic brake grid fan. Keep in mind they were traveling close to 9 mph which is the speed which the manufacturer reports the locomotive's maximum continuous tractive effort. Not saying that's why the car failed but it does correlate timing of the failure. I suppose more obvious proof is the large gap immediately created after the failure. Anyways, lucky catch!

  • @hunter8725
    @hunter8725 7 месяцев назад +1

    Wow, what a catch!

  • @notarotomwithhair5637
    @notarotomwithhair5637 Год назад +1

    When was this recorded?

  • @RFRyan
    @RFRyan 11 месяцев назад +1

    Imagine explaining that to the dispatcher

  • @DESO718
    @DESO718 Год назад +4

    Honestly looks like the car ripped apart.

  • @ScottTaipaleRail
    @ScottTaipaleRail Год назад +2

    Cool catch!

  • @southerncsxvlog
    @southerncsxvlog Год назад +1

    Hope the wreckage is out of the way now. Praise to God it is

    • @rearspeaker6364
      @rearspeaker6364 Год назад +1

      that was an easy 3hr cleanup job. it took more time recrew the train.....

    • @southerncsxvlog
      @southerncsxvlog Год назад

      @@rearspeaker6364 Oh Thank God

  • @SOU6900
    @SOU6900 11 месяцев назад

    Did this use to be a double tracked crossing?

  • @Kiing8284
    @Kiing8284 Год назад +2

    What a catch the chances

  • @hifijohn
    @hifijohn 11 месяцев назад +1

    lucky the train was going slow imagine that at 50 mph.

  • @josephkrizauskas1052
    @josephkrizauskas1052 5 месяцев назад

    Sometimes center pins get old and weak and reach a point where they just shear off. That may be the case here.

  • @caseyvanboxtel2279
    @caseyvanboxtel2279 Год назад +6

    I bet a carman is shaking about losing his job, especially if that car just came from a rip track

    • @erict5234
      @erict5234 Год назад +3

      What carman... PSR got rid of all of the carman!

    • @mshum538
      @mshum538 Год назад +4

      When you dont have “ carman” I guess you have “ corman”…👍~~~

    • @rc391995
      @rc391995 Год назад +6

      That car didn't come from a rip track that's the problem. Lack of inspection and maintenance.

    • @tomt9543
      @tomt9543 11 месяцев назад

      NS has all but shut down mechanical operations in their quest to mimic Hunter Harrison. They’re begging the 100’s of Carmen they unceremoniously dumped in 2020 to come back to work, but the response is almost universally “NO!”. The railroads of this country dug theirselves into 😂a massive hole that they can’t crawl out of when they jumped headfirst into PSR! I spent 41 years as a CARMAN for Southern/NS, and left in mid 2020 after seeing the scorched earth program NS was putting in place! Just sickening

    • @johnblair8146
      @johnblair8146 11 месяцев назад

      8-D@@mshum538

  • @rearspeaker6364
    @rearspeaker6364 Год назад +2

    someone will blame the EMD locomotive at the front for doing this...............

    • @archiebunker7688
      @archiebunker7688 11 месяцев назад +1

      Could have been a spike in the mu plug. The control center at GE can check the feedback from the transponder coordinates between the units and figure what happened.

  • @MainlineSouth
    @MainlineSouth Год назад +2

    Looks like a car was pulled apart

  • @whiteknightcat
    @whiteknightcat 11 месяцев назад +1

    AEX112220 came apart. Looks like a 40+ year old PS4750

  • @paulsmith5398
    @paulsmith5398 Год назад +1

    No, wait.......isnt it a dime theyre supposed to stop on?

  • @funnelfan
    @funnelfan Год назад +1

    Not so much that it derailed, just the slack action ripped the old covered hopper apart.

    • @johnandrus3901
      @johnandrus3901 Год назад +2

      He was pulling at the time, so I doubt that it was slack action. Sometimes a wheel slip can cause a knuckle or drawbar at slower speeds. Didn't really hear that, though.

    • @JointedStudios
      @JointedStudios Год назад

      You did hear that third trailing locomotive go into Notch 8, Right? That probably means it slacked too hard and pulled it apart.

    • @rc391995
      @rc391995 Год назад +1

      You heard dynamic not power .

    • @adipocere1066
      @adipocere1066 Год назад +2

      There are way too many old cars out there. Rusty outside might mean everything under is corroded/rusted too. Half these LO cars look like they belong in Russia.

  • @MeigsCountyRR
    @MeigsCountyRR Год назад +1

    Wow!

  • @rossbryan6102
    @rossbryan6102 11 месяцев назад

    WAS IT AN ACF CENTER FLOW CAR??
    THE WERE BAD ABOUT BREAKING LIKE THAT!

    • @whiteknightcat
      @whiteknightcat 11 месяцев назад

      No. It was AEX112220, an old Pullman Standard car, the one with the blue graffiti that starts to pass the screen at 2:10. Note how the contents (sand?) are pouring out its front end at the very end of the video as the end slope sheet continued on with the car ahead of it.

    • @haroldreardon1407
      @haroldreardon1407 11 месяцев назад

      And why are you yelling with all capital letters?

    • @whiteknightcat
      @whiteknightcat 11 месяцев назад

      @@haroldreardon1407 WHAAAAAT?

  • @rcnelson
    @rcnelson 10 месяцев назад +1

    Start watching at 2:20.

  • @bradleyjanes2949
    @bradleyjanes2949 Год назад +1

    Nilce video

  • @tpep1693
    @tpep1693 Год назад +1

    If you would. have been looking down track, you would of had a decent video.

  • @HDXFM
    @HDXFM 8 месяцев назад

    OMG 😱

  • @SMcCaskill
    @SMcCaskill 11 месяцев назад

    Oooooops!

  • @FirstnameLastname-tp4zw
    @FirstnameLastname-tp4zw Год назад

    Dang😂

  • @joebliss3609
    @joebliss3609 11 месяцев назад

    Aren't you glad that didn't happen at the crossing, while you were standing there filming!

  • @thekingsilverado3266
    @thekingsilverado3266 11 месяцев назад +9

    Every Morning I get up and stretch I know just how that train car feels at my age

  • @mfgc2610
    @mfgc2610 11 месяцев назад +2

    Great catch... No follow up with closer views! Glad it wasn't "running" at speed when this happened. Could have made a bigger mess.

  • @tristanstrains
    @tristanstrains Год назад

    Cool catch Just subscribed too

  • @RHicks
    @RHicks Год назад

    Cool catch!!!!!

  • @mshum538
    @mshum538 Год назад +3

    Where’s the rest of the footage?

    • @chrisrambodiskjockey
      @chrisrambodiskjockey  Год назад +2

      Could not get to it without trespassing and cops and railroad officials were quick to show up

    • @mshum538
      @mshum538 Год назад +2

      @@chrisrambodiskjockey Gotcha bud, thanks~~~

    • @jasonervoes1326
      @jasonervoes1326 11 месяцев назад +1

      ​@@chrisrambodiskjockeylet me guess train knuckle broke. They had to replace it. Couple those hopper cars and then they rolled away.