P0299 lack of power and turbo sticking on a 6.0 Powerstroke F250 diesel

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  • Опубликовано: 23 апр 2011
  • Ford tech explains what causes a lack of power and the P0299 code as associated with the turbo sticking.
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Комментарии • 172

  • @johnballard3334
    @johnballard3334 6 лет назад +137

    Ron is still helping people fix 6.0's from heaven!

    • @hazzmatt84
      @hazzmatt84 2 года назад +6

      3 years after this comment, I still seek out his videos every time I'm having issues with my 6.0. this man was a hero. Such a shame.

    • @rossosborne8858
      @rossosborne8858 Год назад +1

      Amen.

  • @thinkfirst6431
    @thinkfirst6431 6 месяцев назад +8

    All these years later Ron is still the first place I go to for information. Hope that the family is doing well and still getting something from Ron's vids.

  • @stearman
    @stearman 8 лет назад +96

    Rest In Peace Ron. We all appreciate your help.

    • @travisandmissydog
      @travisandmissydog 8 лет назад +1

      Did he pass??

    • @zingzong5
      @zingzong5 7 лет назад +1

      Travis Bennett yes, car crash

    • @TurboGfx16
      @TurboGfx16 4 года назад +1

      😪

    • @TurboGfx16
      @TurboGfx16 4 года назад +4

      @@zingzong5 Yea, so horrible! I heard that it was a stupid teen driver, that crashed into Ron. 🥺😥

  • @danieljandt6981
    @danieljandt6981 6 лет назад +26

    Ron you are very much missed, you are a special person when you were here. I hope God has you in his hand and give you peace and love. Miss you Bud.

  • @dawsondemontiney1247
    @dawsondemontiney1247 Год назад +7

    Man I wish I could've met this man. 😪 it breaks my heart knowing he's past but he's made an incredible impact on the diy or pro mechanics. Thanks Ron for your knowledge and know it is greatly appreciated

  • @franciscovera828
    @franciscovera828 5 лет назад +4

    Ron is still fixing trucks out here in Mexico!! We miss u Ron- descansa en paz

  • @firsttimediesels6289
    @firsttimediesels6289 2 года назад +1

    Thank you Ron, rest in peace man I don't know where I'd be without these videos.

  • @dirtypocketsct
    @dirtypocketsct 5 лет назад +8

    Ron always learned from your videos. You were a big help with a lot of my early 6.0 problems. Thank you and RIP.

  • @clintroughton1423
    @clintroughton1423 7 лет назад +14

    Nice videos Ron! I feel as if I work on my own trucks its like paying my self $85-$125 per hour. I don't understand how people can afford NOT to work on there own stuff. Keep up the good work!

  • @Sara_The_Feral_Housewife
    @Sara_The_Feral_Housewife Год назад

    Didn't find Ron's videos until after his passing. So thankful for him teaching me about my turbo!

  • @jeremyandholly2011
    @jeremyandholly2011 6 лет назад +3

    Gone but not forgotten. Thanks for all you did Ron.

  • @anthonyariza8215
    @anthonyariza8215 7 лет назад +3

    Best 6.0 videos on the planet Rest In Peace diesel master

  • @blliverm
    @blliverm 2 года назад

    Thank you Ron. You have helped thousands of people save money and be grease monkeys on the weekend.

  • @MrSouthwestvoodoo
    @MrSouthwestvoodoo 6 лет назад +2

    You sir are a legend and grateful for your contribution to your local community #rip #thankyou #dieseltechron

  • @edotis3389
    @edotis3389 2 года назад

    You don't know what you got, till he's gone. So many questions I need to ask you.
    Never met you, but I miss you Friend ♥️

  • @lexusry
    @lexusry 8 лет назад +1

    WE NEED MORE GUYS LIKE HIM, SHARE REPAIR EXPERIENCE

  • @stevemooers5501
    @stevemooers5501 10 лет назад +2

    excellent video, thanks for taking the time to record it and great job explaining.....

  • @bertdownton
    @bertdownton 11 лет назад +1

    Hi, we had 6 codes related to low turbo boost, we cleared all codes & code came back as P0299 low Boost, first thing we did was check the intercooler, right side of the intercooler was leaking very badly & would not hold pressure, we changed the intercooler & roadtested, we still had lack of power with turbo fart on hard acceleration, removed turbo, vains were stuck, cleaned turbo, checked operation no good, found roll pin broken in actuator, fixed pin & cured problem, thanks for the video.

  • @tosborn62
    @tosborn62 7 лет назад

    great video answered my question. Miss you Ron i will remember you and your wife and kids in my prayers. God bless.

  • @morrislucero810
    @morrislucero810 Год назад

    Thank you Ron. Wish you were still here. See you some day

  • @FordTechMakuloco
    @FordTechMakuloco 10 лет назад +10

    Good stuff dude!!

  • @sledhead904
    @sledhead904 6 месяцев назад

    When you see this outfit you know you got a real deal classically trained mechanic. Rip man

  • @rogerdrum5936
    @rogerdrum5936 7 лет назад

    Thanks for the video.
    2006 6.0 4 x 4 with 201k miles.
    Still love this truck!

  • @russellhartley1882
    @russellhartley1882 9 лет назад

    Ron, Great video and advise. Keep the videos coming I have learned a lot.

  • @25yearfleettechnician63
    @25yearfleettechnician63 4 года назад +1

    RIP Ron. Thanks for all the help along the way. Split our oldest 2003 6.0 turbo today. Barking, performance code. Unison ring was real tight. Cleaned it up real good. Minor pitting. Unison wheel was in fine condition otherwise. 173k. Actuator slot not oblonged etc. Pretty certain I had improved % on VGT data also. Like it wasn’t fully functional prior to cleaning.

    • @Trev619
      @Trev619 Год назад

      Did that take care of your turbo barking and performance

    • @25yearfleettechnician63
      @25yearfleettechnician63 Год назад

      Yes. Pretty common. I’ve done a few now.

    • @25yearfleettechnician63
      @25yearfleettechnician63 Год назад

      You can pull the VGT actuator and use a magnet or a pick ( I forget now ) and move the unison ring pretty easy when it’s working properly. Plus you can do this before and after cleaning to see the difference. In fact I’m sure Ron shows how to do it

  • @trainer2018
    @trainer2018 10 лет назад

    Great video Ron. This will help me out. We work on quite a few Power strokes at the shop I work at. Thanks.

  • @FordTechMakuloco
    @FordTechMakuloco 10 лет назад +12

    Don't forget a plugged map port can cause a P0299 code as shown in my P0299 video.

    • @redman1716
      @redman1716 9 лет назад

      What about blow back under hood , like smut. Is that a sign of a bad turbo or FCIM

    • @FordTechMakuloco
      @FordTechMakuloco 9 лет назад

      turbo flutter you mean

    • @waynewilliams1922
      @waynewilliams1922 9 лет назад

      FordTechMakuloco is there need ever for a blow off valve?

    • @johnlewis6642
      @johnlewis6642 3 года назад +1

      I'm stumped on mine. No code set but taking off from a dead stop it lags, the VGT goes up and not down.. On hard acceleration it will go to 85% then drop to say 30% or whatever and that's when it accelerates.. Blows plumes of black smoke.. Changed my VGT actuator but no difference. Also, going down the road about 50-70 mph I try to accelerate, it will miss until I let off the gas and hit the gas hard again it will take off. Haven't taken the turbo off yet.

    • @a-aronsendthebiscuit541
      @a-aronsendthebiscuit541 3 года назад

      i had all this problem. nd when it came back from mechanics it only made 15 psi max boost. did all sorts of forum researches. ended up being a clogged map sensor line. i drove myself wild trynna figure this out! new line and a thorough cleaning and it hauls ass!!

  • @jtho8019
    @jtho8019 Год назад +1

    I was worried I might need to replace my turbo as Ron said that if Unison ring stuck on its mounting and wont turn you might have to replace it. I attacked it with a die grinder and wire brush and 3M roloc wheels. These helped but still left behind a lot of corrosion. After taking a Goodson carbide super scraper to the hub where unison ring seats and the area underneath where the ring mounts it cleaned up real nice and now the unison ring moves freely. It also worked great on the mating surface of the two halves of the turbo which were heavily corroded. Just take your time with it and dont leave gouge marks. Work with a shallow angle so as not to dig in.

  • @travelinnate2761
    @travelinnate2761 5 лет назад +1

    Great video Ron! One of the greats gone to soon. Rip

  • @nickayivor8432
    @nickayivor8432 2 года назад

    SUBSTANTIAL DieselTechRon
    We miss you
    Thanks 👍
    DieselTechRon
    From Nick Ayivor from London England UK 🇬🇧

  • @DieselTechRon
    @DieselTechRon  11 лет назад +4

    Cleaning is easy with the proper tools. If you're able to remove it and more important install it back properly than cleaning it is easy. I read people commenting on the anti seize. It's only for assembly. It's gone once it warms up. By far the most common cause for failure is short driving times not burning the condensation and moisture off.

  • @brianmorral9072
    @brianmorral9072 3 года назад +1

    Rip Ron your a good man!

  • @JohnDiMartino
    @JohnDiMartino 10 лет назад +1

    Great video,thank you for sharing.

  • @YahikoHaldane
    @YahikoHaldane 11 лет назад

    Thank You for the alignment tips

  • @jasonskinner1555
    @jasonskinner1555 9 лет назад

    Love these videos save me money!!!

  • @wesrr4036
    @wesrr4036 5 лет назад

    Miss this guy!

  • @stevensimmons510
    @stevensimmons510 10 лет назад +1

    Thanks...great video!!

  • @thecarbaddie
    @thecarbaddie 7 дней назад

    Thanks for the help. RIH ❤

  • @ryanweems8310
    @ryanweems8310 11 лет назад +1

    Thanks for the video, it worked great.

  • @austinatkins408
    @austinatkins408 5 лет назад

    You’re the man Ron, saving my bacon time after time. RIP sir.

  • @AcuraJ32
    @AcuraJ32 9 лет назад +9

    Wow this guy knows his shit! Keep up good work love the video.

  • @victorsoto777
    @victorsoto777 7 лет назад

    He did very good videos I recommend people to watch his videos.

  • @jjwoodford2941
    @jjwoodford2941 9 лет назад

    Thank You!

  • @petroman-de7vm
    @petroman-de7vm 9 лет назад

    Great videos,thanks! I have a ? I've searched all your videos and I don't think you mention the actuator. Does that go bad?

  • @Kanesgarage
    @Kanesgarage 13 лет назад

    Wow, these are great videos! Very good information. Do you work much on the 6.4's?

  • @OscarRodriguez-bi1jv
    @OscarRodriguez-bi1jv 8 лет назад +1

    hi ron, will the truck smoke a little after putting anti seize in the turbo?

  • @YahikoHaldane
    @YahikoHaldane 10 лет назад

    Ron,
    Any reason to not use a media blast cabinet to clean the the outer housing?
    Also if you do what would be the better media to use Sand,Glass or Walnut?
    Thanks

  • @JimChristiansen
    @JimChristiansen 10 лет назад +1

    Hello Ron. I very much appreciate your videos. Thank you.

  • @TheWaelabo02
    @TheWaelabo02 7 лет назад

    thank you

  • @petersmith5722
    @petersmith5722 10 лет назад

    Ron,
    Thanks for all the helpful hints. I recently replaced the turbo on my 6.0. The truck runs great, however under a heavy load with no loss of power it will throw a PO299. The turbo pressure on the instrument cluster will indicate good positive pressure and the scan gauge would show a negative boost, VGT will also drop below 15. All seems normal when the load lightens up a bit. Please help. Any Idea ?

  • @anthonyhill503
    @anthonyhill503 Год назад

    We miss you

  • @Mohammadhoeslaying
    @Mohammadhoeslaying Год назад

    Thanks Diesel tech Ron

  • @johnsonshomeimprovement7067
    @johnsonshomeimprovement7067 9 лет назад +1

    Hay Ron i have a 2006 f350 6.0 runs vary good but sometimes it has a lite miss or skip when you have lite load no codes

  • @hondamojo1
    @hondamojo1 11 лет назад

    Most all the turbos Ive done, the antisieze burns away in a relatively short period of time anyway. The problem lies when you glob it on .Use sparingly if at all.

  • @terrylease9609
    @terrylease9609 8 лет назад +7

    Hey diesel tech Ron I just bought a 04 6.0 the vgt at idle is 85 but at 70 it's around 53 but I'm only able to build 18psi of boost I think from exhaust sounds my veins in the turbo are stuck

  • @chrishardin8064
    @chrishardin8064 Год назад

    Sbig shout out to DTR he showed me how to do my injectors and how to take a turbo out in less than an hour much respect

  • @mikesbb77
    @mikesbb77 8 лет назад

    I have a real issue with my 07 6.0 PSD when at a wide open throttle, fully warmed up and under medium to heavy load, I'm getting a popping through the intake noise and a loss of power... I'm in the process of pulling the heads off to replace bolts with studs and new bulletproof EGR cooler and engine oil cooler. The cylinder heads checked out good(no cracks, pressure tests and perfectly straight) I'm hoping that when it's all back together that the "popping" is gone. There were no stored codes and I had plenty of boost. While the turbo was off I tore it down and cleaned it, all the working parts moved smooth and easy. Is there anything that you can suggest before I put it all back together?

  • @VanessaSilva-ux6uk
    @VanessaSilva-ux6uk 2 года назад

    Awesome video. I took my dad's identical turbo apart and the plate was stuck. I took a wire brush and cleaned up very well, added some anti-sieze, reassembled, checked with a magnet for movement.....all good, reinstalled turbo. It sounded great and truck fired right up but after driving for a day, went to pass and lost power. Not sure what happened. Maybe something got disconnected. Any thoughts?

  • @MetalheadX45
    @MetalheadX45 10 лет назад

    Ron, I've got a check engine light on my 06 6.0 the other night after a cold start and I tried to read it but it said no codes. I deleted it and got it again the next day and it said p0000. The truck doesn't run rough and idk what the hell I could be, I'm thinking if anything the ficm is bad cause it's getting hard to start since it's been cold

  • @jacobkrell6795
    @jacobkrell6795 5 лет назад

    He was the man. RIP

  • @daddy-daughterdays8169
    @daddy-daughterdays8169 6 лет назад

    THANKS

  • @alejandrovillacana3544
    @alejandrovillacana3544 6 лет назад

    MUCHAS GRASIAS MAESTRO DICEL POR SU VIDEO ES EL MEJOR EN TODO EL MUNDO MUY BUEN TRABAJO COMPA MUY BERGA Q ES USTE

  • @1693caterpillar
    @1693caterpillar 10 лет назад

    Hi Ron: Is it possible, to check the vane movement of the vanes, through the port with the threaded plug, while the turbocharger still mounted on the vehicle. Thanks...

  • @cs31-916
    @cs31-916 2 года назад

    f250 turbo 6.0 ran fine just before the 0299 code; took turbo apart and disc/viens were ceased so got them cleaned up very well and applied anti-sieze, reassembled and checked with magnet and moved back n forth. Installed turbo, and reconnected all. Drove for a day and on second day took it on the highway, wen to pass a car and lost power. Very demoralizing. It's my dad's truck. I haven't looked at the truck to see if something came loose but curious if you had any thoughts.

  • @davecozzi6937
    @davecozzi6937 8 лет назад +1

    Does a stuck on unison ring mean replace the turbo or is it ok to change out the unison ring?
    Hello Ron thanks again for all the great videos. I just disassembled the turbo and the unison ring was really stuck on. Had to pry it off like you said. The actuator hole looks ok but this my first so not sure. Does a stuck in unison ring mean replace the turbo or is it ok to change out the unison ring? I have a 2003 Excursion 6.0. It was blowing off through the intake ("barking" "huffing" don't know the term) while accelerating, and when I let off it would chatter air sound. I had a p2285 but I changed the ICP and harness a couple moths ago and while in it right now it looks good no leaking. The IPR pigtail was frayed on both wires. I've spliced in a new pigtail for that and have put the new screen and gasket set on it. Thanks for your time sir!

    • @DieselTechRon
      @DieselTechRon  8 лет назад +3

      replace it if it's worn. Check where the shaft moves it and the vanes slide. Make sure to clean the hub too. It must move freely.

    • @davecozzi6937
      @davecozzi6937 8 лет назад +1

      +DieselTechRon thanks a lot! I'll clean it up real good and put in a new unison ring. Thanks again

  • @derekallendraper5076
    @derekallendraper5076 8 лет назад

    Could a problem with the low pressure fuel pump on the frame rail cause this code to set?

  • @patgiles2462
    @patgiles2462 10 лет назад

    So what is wrong if I now have a oil leak? It seems like I had to loosen the clamp just a bit to allow the auctatior to move and now the leak began.

  • @TheIrfanxz44
    @TheIrfanxz44 12 лет назад

    Can you use regular multi grease for the vains or it has to be that stuff you used

  • @mikemitchell3142
    @mikemitchell3142 8 лет назад +2

    CETANE rating of 45 is the Minimal for Fords and its crucial! Most diesel fuel in the US has a rating 38-40, not enough for Fords. Low Cetane ratings will cause silt build up and cause your EGR's to gum up and fail.

    • @yo6488
      @yo6488 7 лет назад

      Here in Cali its 50 if I remember right

  • @jasonskinner1555
    @jasonskinner1555 9 лет назад

    You could sell that snap on tool box and live like a king for the rest of your life lol

  • @MechanicTechnicianRepair
    @MechanicTechnicianRepair 7 лет назад

    good diagnostic. amigo. tengo. una. pregunta. amigo

  • @Zero12495
    @Zero12495 8 лет назад

    do you have a turbo rebuild video? :} @dieseltechron

  • @utoobrandomness7197
    @utoobrandomness7197 8 лет назад +1

    Over the weekend, I tore into this project & got to the part in reassembly where Im pulling the seal for the oil operated piston that moves the actuator rod & it wasnt moving using a magnetic parts grabber like youre using.
    I was working outside & it started snowing, so I moved things into the garage & this piston fell out in the process, I put it back in -seemingly it had a full range of motion, I reassembled the exhaust side to the center housing & reattempted the magnetic parts grabber on the piston while shining the light into where the Y pipe hooks onto & could see the vanes moving.
    Ive now got everything back on & the truck fires up, but it seems really reluctant to build boost, maxes out @ ~10psi, and has some funny sounding harmonics.
    I think my alignment for the piston & the actuator rod went less than great -How would I go about checking this? :)

    • @DieselTechRon
      @DieselTechRon  8 лет назад

      Hi. Sorry for the late reply. I have a video about power loss after turbo repair showing how to index it properly. also the ring sticks on the hub.. I should have shown cleaning that TOO

    • @utoobrandomness7197
      @utoobrandomness7197 8 лет назад

      +DieselTechRon No worries, Thanks for replying :)
      This weekend I had the opportunity to tear the turbo off again & reindex the piston/plunger to the actuator arm. After having put everything back together, it still seems like Im not really getting that much boost (engine sounds from the previous time apparently were not getting the downpipe completely mated up to the turbo); At the moment DTC-wise Im getting P1000, P0113, and P0487. Would any of these cause the turbo to make a more minimal output?

    • @kaylawipf3371
      @kaylawipf3371 7 лет назад

      UToobRandomness

  • @CollinSmithRealEstate
    @CollinSmithRealEstate 6 лет назад +1

    Would anyone happen to know if a faulty plunger would have a negative impact upon reassembly? The actuator rod from the oil plunger makes a gargling noise and is difficult to move back and forth when i rotate the unison ring. Is it normally pretty hesitant to move, or is the pluner not operating as it should?

    • @LynxStarAuto
      @LynxStarAuto 5 лет назад

      TheTruckFanatic actuator failure. Unfortunately, you need a new turbo friend.

  • @ArmandoRodriguez-vi4lo
    @ArmandoRodriguez-vi4lo 8 лет назад

    Hi Ron I have i2005 F350 sounds like it has a air leak coming out from the turbo when I disconnected electrical wire that a hook up to turbo stops sound of air leak will stop is there any way that anybody can tell me what this can Be the problem

  • @walterpuchuri1524
    @walterpuchuri1524 Год назад

    Dios LP tenga en su gloria gracias maestro

  • @rogermatsuo5739
    @rogermatsuo5739 9 лет назад

    Gentlemen, question? I have a 05 6.0 diesel, Check engine light is on. I have cleaned the ERG valve, Checked the air line on the manifold by the map thing, also replaced a top hose that was cracked. reset service light, light is off. now the problem is that the top turbo hose keeps blowing off, there was no oils or anything that was put on the hose, only carb. cleaner and cleaned all the connecting fitting. now it seems that I have way to much pressure, the top hose keeps blowing off upon heavy acceleration or when towing, what am I missing, is there anything that I need to check? I feel that it a sensor somewhere, thats my feeling. the turbo to me feels fine. but I'm not a Diesel tech. so if anyone has experienced this please help me thank you.

  • @joseguerrero9972
    @joseguerrero9972 9 лет назад

    Ron I got 06 ford 6.0 got code p040 & p299 vgt is at 41.00 is this normal

  • @mark.r8900
    @mark.r8900 11 месяцев назад

    Hi, my wastegate is shut closed tight. The actuator is not holding pressure causing the wastegate flapper to be stucked closed. But I don't know why I am getting a P0299 underboost code. If wastegate is stucked closed shouldn't i be having overboost ? The car runs but has no power slow acceleration. Any help would be greatly appreciated. Thanks

  • @inerfyr
    @inerfyr 11 лет назад

    Does it matter what kind of anti seize I use on the turbo?

  • @tinok.8149
    @tinok.8149 Год назад

    LegendRIP

  • @colesiebenahler8168
    @colesiebenahler8168 2 года назад

    My 05 f-250 want to rev the turbo when not needed like 50mph and below is good but once you step on it a bit to get going it want to do like a constant rev and sometime will cut powers of the turbo get to high when doing it but then jump backs on

  • @keithmoulding9671
    @keithmoulding9671 11 лет назад

    what cases the heavy pitting on the veins ?

  • @muensterfactory3940
    @muensterfactory3940 9 лет назад

    Ron
    I got my turbo off and when I pulled it apart, the unison ring was definitely stuck and I had to pry it off. The unison ring looks fine. Do I need to get a new turbo or is there a way to free the unison ring?

    • @donid6660
      @donid6660 9 лет назад

      Same issue here... I just sanded and cleaned the place where it was stuck on - it was rusty. So i will start putting it together now and see how it goes

  • @Silverspank
    @Silverspank 12 лет назад

    Would that be a covered warranty item?

  • @hill392
    @hill392 2 года назад

    Still the best.

  • @leaiconn1925
    @leaiconn1925 9 лет назад +1

    Hi Ron I have an f350 6.0 that starts fine just takes a while I'm talking half hour to worm up any idea.. it's runs fine after wormed up. If I start and let it worm up for 5 minutes and try to drive it feels like it's missing. But if I let it worm up for 30 min. She runs amazing. Idk if this help but it's a standard transmission. .

    • @wireboy253
      @wireboy253 9 лет назад +1

      Fuel injector stickion

    • @rochanmohyalsharma2406
      @rochanmohyalsharma2406 8 лет назад

      It must be taking longer self starts.

    • @mikemitchell3142
      @mikemitchell3142 8 лет назад

      +Leai Conn Have you figured it out? I have a few questions for you if you haven't fixed it yet

    • @wireboy253
      @wireboy253 8 лет назад +1

      Mike Mitchell Fixed mine recently same symptoms fixed with new injectors.

  • @MB-ht9rb
    @MB-ht9rb 3 года назад

    I am a no one who has just watched a few videos over the years. I am sorry he passed so young.

  • @maylnwood
    @maylnwood 8 лет назад

    I have an 04 6.0 powerstroke. I have noticed a weird clattering(low pitch) noise. It's not consistent. It comes and goes, usually about 10 seconds and it will stop.. It doesn't sound like a knock so I don't think its a lifter(at least I am hoping to god that its not a fucking lifter) someone said it could be the turbo sticking or a leaking intake. Could something like that make noises like I'm describing?

  • @luislow9586
    @luislow9586 10 лет назад

    Hi Ron, I have 2002 6.0 powerstroke F450, in my turbo charge I see there is oil inside the turbo and go inside the exhaust down pipe, when I start the engine there is a lot white smog, how I can fix this. Thank you,

    • @laserblast92
      @laserblast92 9 лет назад

      Turbo vane shaft seals are leaking, replace turbo

  • @chrisX96X
    @chrisX96X 11 лет назад

    got a code of p2262 turbo boost not detected whats the fix for this problem thanks

  • @richardmathers7238
    @richardmathers7238 3 года назад

    Does dirt or carbon only build on hot side

  • @curtleake2191
    @curtleake2191 9 лет назад

    Hi Ron, Love the videos but can't find my problem. I get the PO299 but the truck runs like new with no problems. I have a new EGR valve, new MAP, new sensor under the Degauss tank(can't remember the name) and only a CEL. It will run for days then throw the CEL. It runs about 25# of boost. Any ideas? 57K 50% pulling 16k trailer.

    • @curtleake2191
      @curtleake2191 8 лет назад

      +Curt Leake Unison ring was stuck to the center.

    • @LynxStarAuto
      @LynxStarAuto 5 лет назад

      Curt Leake nice!

  • @janstrzelecki7967
    @janstrzelecki7967 2 года назад

    Hi,could you tell what is happened I start the engine cold and was running 30-40 minut good I stop engine for 3-4hours than I start the engine and show me low oil pressure where i have to look to find problem

    • @amazingwonderwoahman5465
      @amazingwonderwoahman5465 2 года назад

      I have low oil pressure unless I give it throttle. It smokes, has no throttle response at first, check gauges light also came on. It smokes so bad as well

  • @hondaridered29
    @hondaridered29 11 лет назад

    holy S*** thats a HUGE TOOLBOX!

  • @6literfuelaholic655
    @6literfuelaholic655 2 года назад

    Why dont you anti seize the unison ring?

  • @jessicalopez2597
    @jessicalopez2597 9 лет назад

    i have a 2005 ford f350 dually 6.0, it started fine i went from utah to california, on my way back the rpms started to drop like crazy and when i acelerate kind of white and blue, it shut off on the freeway and i started back up and samething happend, i let it cool off and now it doesn't start, any recommendations

    • @rochanmohyalsharma2406
      @rochanmohyalsharma2406 8 лет назад

      Oil pump damage.
      It heppens due to Bad quality of engine oil or low level of oil in the sump so at high speed when flow of oil is max inside engine, oil pump begin to suck air. This lead to damage engine and turbocharger.

    • @utoobrandomness7197
      @utoobrandomness7197 8 лет назад

      +Jessica Lopez Had the same thing once upon a time going thru Wyoming, come to find out the STC fitting ate it & high pressure oil system was not holding high enough pressure

    • @LynxStarAuto
      @LynxStarAuto 5 лет назад

      Definitely sounds like an internal leak of the oil system. The fuel injectors on these depend on oil pressure to function properly. I know it has been 3 years, but for anyone reading this, check out your oiling system. Pull the valve covers and inspect the oil pressure rail. I would start there.

  • @luissrangel390
    @luissrangel390 3 года назад

    I have a 2006 6.0 F350 and I have smoke coming from the exhaust and vibration while idling/driving and won’t go over 55mph and struggles to get boost power and turned off lost all power while on the road could be bad injector or my turbo gone bad? Any conclusions?

  • @karadenise22
    @karadenise22 9 лет назад

    Hey do you have any idea why my turbos would flood with oil? I have a 2006 f250 6.0. Apparently the mechanic at the dealership has no idea but this it should cost 6k to fix.....

    • @bobbymoore6328
      @bobbymoore6328 9 лет назад

      karadenise22 The most common thing I have run into, as far as excessive oil in the turbo, is blow by coming from the crankcase breather on the valve cover. This is connected directly to the inlet hose to the turbo by a small hose from the breather on the valve cover.

    • @utoobrandomness7197
      @utoobrandomness7197 8 лет назад

      +karadenise22 In the center housing, theres a little ring (like a piston ring) that plays the role of a seal in the cavity where lube oil comes in to lube the turbine shaft; Its possible that seal/ring has gone to shit? If you dont want to tear into it,Try taking it to a turbo shop & see what they say. The amount of oil from the CCB like theyre talking about below is going to be pretty minimal...

  • @jimrozkhan3236
    @jimrozkhan3236 2 года назад

    We’ll let me start by saying my turbo was making small noises of something grinding inside while I was driving , I don’t know why but I accelerated down thinking it would fix the issue but instead my truck started blowing bluish white smoke and ran for a little bit and ended up shutting off, and it leaked out a lot of oil during that time it leaked out on the passenger side of the truck looked like the smoke could possibly been from oil in the exhaust (2003 Ford F-250 6.0). Now it won’t start , and is showing a p132b code . A mechanic came with another computer and is claiming piston 5 is misfiring as well. Has anyone ever experienced this ? Or have any idea what it maybe? I don’t want too invest in all kinds of parts for no reason that’s why it’s important for me too find out what the issue is .