UPDATE: iNav PID Tune fix for the Flywoo Explorer LR 4" FPV Drone with iNav
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- Опубликовано: 18 сен 2024
- This is an update to my previous video where I upgraded the GPS and flashed iNav to my Flywoo Explorer LR 4" quad. I had issues with the quad pitching down when yawing with a slight roll added to it. This is what i did to fix that issue.
Here is the First video: • Full Install Guide: Ne...
Glad you got it flyin right.
Excellent video.... I did something wrong and when I couldn't recover the "dump files" from my old computer.... were can I get those files for flywoo explorer HD LR4 version 1 with caddx vista... Thank you.
Please make more Flywoo Explorer videos
How did you get the magnetometer working ? I got a iflight v2 gps/compass all wired up check continuity on scl sda all good gps works fine both mag sensor dead ram cli status states magnetometer unavailable frustrated also would love your inav cli dump haven’t even tried to arm it yet stupid mag not working
I had the same issue. I was flashing the wrong firmware. I was flashing the FLYWOOF745 instead of FLYWOOF745NANO.
what a about the flight time,sir ? is still efficient with inav, or not ?
Not sure yet, I have not done a flight time test yet, just getting the tune all set in. I will have a flight time test coming soon
Do you put the Lion on the bottom because of the weight?
Actually I mount it on the bottom to free up some room on top, I sometimes put my Action 2 on this quad and the space on the top is pretty sparse. DOesnt seem to effect it any
why did you choose inav instead betafligth?