Gear driven 50dn alternator spectacular fail in a detroit diesel 8v71.

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  • Опубликовано: 22 окт 2024
  • Boy did this ac delco 50dn gear driven 24v oil cooled alternator fail on this detroit diesel 8v71. Lucky failure could have been so much worse.

Комментарии • 108

  • @greglammers9905
    @greglammers9905 Год назад +21

    That’s one lucky bus owner. I did a LOT of those in my day. I only had one drive take out the gear train in 43 + years of working on buses.

    • @BusGreaseMonkey
      @BusGreaseMonkey  Год назад +12

      Usually that’s a gm problem. This is the only mci i have ever worked on with a gear driven alternator. They always have air tensioned belt drive alternators

    • @greglammers9905
      @greglammers9905 Год назад +14

      @@BusGreaseMonkey I was always going to get you a couple of these alternators. I have a gear driven one from an MCI 8v71, and a belt driven one from a Prevost XL series 60. If I ever get down your way, I’ll drop them off. When you were up in Minnesota at Stan’s shop a few years ago I tried to get up there but it didn’t work out.

    • @greglammers9905
      @greglammers9905 Год назад +1

      @@BusGreaseMonkey I took the 50dn off my bus (1995 Prevost xl series 60 Detroit) and replaced it with a duel setup 140 amp 24 volt Bosch and a delco 200 amp 12v for my house batteries. I took all the bus HVAC out except the front defrost and air

    • @marksmith-ew7ir
      @marksmith-ew7ir Год назад +1

      The owner was very lucky

    • @gregallen7045
      @gregallen7045 Год назад +2

      Rest of thing’s looking kinda sketchy
      Owner needs to up his game on prevention maintenance maybe

  • @gregchamberlain3276
    @gregchamberlain3276 Год назад +10

    The folks that own these buses are really Fortunate to have a company like yours to repair and inspect them. If I owned one of these buses, yours is the only place I would bring it for service. .Keep up the great video's please.

  • @brucemcgee2281
    @brucemcgee2281 Год назад +3

    I used to rebuild Delco and Leece-Neville starters and alternators when I was younger in Atlanta. This is a very interesting topic to me. Thanks for letting us watch.

  • @18robsmith
    @18robsmith Год назад +4

    Ah the joys of oil-cooled motors & generators.
    Great when they are running well, but oh dear me, how messy when they stop, particularly with gear/shaft drives. Last one I worked on suffered a winding failure which seized the machine (at least there was a shear-pin in the drive shaft so the diesel didn't break). We drained the oil and copper filings from the machine before stripping it using filter pads to collect the debris (we did a full failure analysis as there were several similar failures at the same time), then wash the residue out (more bits of copper). Finally located the source of the failure - incorrect taping and balancing of the windings leading to the rotor hitting the stator, the debris caused a bearing to fail and, as they say, the rest was history. A batch of about 80 generators was recalled (or at least those that hadn't destroyed themselves) and all were found to be heading down the road to destruction.

  • @1982MCI
    @1982MCI 11 месяцев назад

    Hey Scott, this was a great video that helped me with my 50d generator issue on my MCI. Thanks Scott!!

  • @robp7652
    @robp7652 Год назад +4

    Also you are so correct about that bearing. I had a Jabsco pump on the back of a 4 71 that was missing a little bearin retainer for when it does go bad. The gear drive does not like ball bearings. Not one bit.

  • @randyclyde4939
    @randyclyde4939 Год назад +2

    I've never seen THAT before! Good grief... Thank goodness they found BGM! Be well, be safe!

  • @rickykeaton9236
    @rickykeaton9236 Год назад +1

    That burn up spot on the alternator was probably caused by the original wires that were replaced with that new red wire

  • @uncmouse
    @uncmouse Год назад +1

    found it,was in community section.wife ill and my brain is frazzled.further look at that debris in pan tells me internal damage to driven gear in engine.those are pieces of gear teeth.ruh oh.as said if they arent lined up this happens.now theres your meow mix from engine.memories from my days at domenico tours .

  • @GNX157
    @GNX157 Год назад +5

    Wow that alternator looks super heavy duty. I can only imagine what it costs to replace it.

  • @bwalker4194
    @bwalker4194 Год назад

    Absolutely love hearing that big 2-stroke sing!

  • @normanott644
    @normanott644 Год назад

    I have overhauled several 50 DN units , on large motor homes. I built a jig for my tester to run it up for testing. It’s an interesting unit, oil cooled high output. I haven’t seen one in a while.

  • @claytoncoolidge992
    @claytoncoolidge992 Год назад +6

    Man that is lucky. Though Scott I hate to go against your thought but I would be extremely hard pressed to be convinced that melted aluminium is the cause of the failure and whatever shorted it out either damaged or welded a ball or 2 in the bearing and came apart. That's all too much damage and fresh looking enough to be coincidence and whatever happened isn't on the hot side of the system. There's a massive ground issue and the oil line became a high current ground

  • @delsloat9130
    @delsloat9130 Год назад +5

    Original wire was probably shorting on spot ware red wire was stuck

  • @abpsd73
    @abpsd73 Год назад +2

    "A bunch of screaming cats" is never a sound you want emanating from your engine bay. It would make sense that the bearing behind the drive gear should be a tapered roller to handle the radial loading force of gear mesh, once the ball cage is deformed and spit out, it's game over.

  • @michaelovitch
    @michaelovitch Год назад +2

    If the bearing transmits the short circuit caused by the red wire,it will damage the balls and race,so cause the bearing failure.

    • @Wayoutthere
      @Wayoutthere Год назад +1

      Aah nice one, yes that might indeed have happened. Arcing digging pits in the ball bearings, grease flowing out and BAM. Why you should never weld broken equipment with bearings still in them.

    • @joehead1294
      @joehead1294 Год назад

      @@Wayoutthere Go tell that to those pakistani boys. LOL...

  • @motorcoachtech7615
    @motorcoachtech7615 Год назад +4

    He was very lucky. Do you think the drive gear on drive train is centred in the housing? Maybe putting side stress on alt gear? The damage at the oil fitting looks like the 24v lug broke off one time, and was bouncing and shorting on case.

  • @grumpyg9350
    @grumpyg9350 Год назад

    As always, nice close ups.👏🏻👏🏻👍👍

  • @jeffbyrd7976
    @jeffbyrd7976 Год назад +3

    I have had 24 volts blow the end of a large screw driver. I would not be surprised if it did that to aluminum.

  • @RollerCoasterLineProductions
    @RollerCoasterLineProductions Год назад +1

    I know what happened. The cable rubbed thru, arced, grounded out and deposited a small piece of metal in a small gap somewhere inside the alternator and eventually made its way to thru the bearings and ruined it.

  • @SuperMAZ007
    @SuperMAZ007 Год назад +1

    That rebuild alternator looks sus specially with all that red rtv silicone.
    That is also one lucky bus owner only a inch away from a total catastrophy.

  • @jamesallen712
    @jamesallen712 Год назад

    Wow. That was a very lucky ball! Hate to think what the repair bill would have been if had not done what it did. Something different thats for sure.

  • @larryanderson8049
    @larryanderson8049 Год назад +2

    Lucky Dog just being lucky..

  • @uncmouse
    @uncmouse Год назад +2

    what happened to the vid of debris found in the oil pan of this bus,left a comment .but wheres the vid

  • @sal3060
    @sal3060 Год назад

    That bus owner is livin' right. Voof.

  • @firemedicseven
    @firemedicseven Год назад +1

    Is there a work around to put a regular belt driven alternator on there to get away from the possible gear train damage or is it even necessary? I assume that style of alternator must be pretty reliable or you wouldn't be putting it back to stock.

  • @christophermarsh6983
    @christophermarsh6983 Год назад

    Goddamn do I hate that wrestling the alternator through the side door bullshit. Laying on your stomach over the corner of the hatch trying to wrestle that thing back into place. Nah, glad Im done with 2 stroke buses.

  • @johnny22single99
    @johnny22single99 Год назад +1

    ABSOLUTELY----> AWESOME!!!!!!!!!!. 🙂

  • @barryk8969
    @barryk8969 Год назад

    Electrolysis has been rampant

  • @davefroman4700
    @davefroman4700 Год назад

    Guy has a couple horses in his back pocket. Thought for sure the mating ring gear was going to be destroyed.

  • @bat__bat
    @bat__bat Год назад

    Strange one there. Hilarious part is that something chewed up that aluminum bc it ain't a fantasy. 🚌 💨

  • @davidowen888
    @davidowen888 Год назад

    Quite peculiar alternator issue 🧐 BGM investigator 🤓☮️

  • @Realroyrogers
    @Realroyrogers Год назад

    I love the hill climbs

  • @garyharrington5300
    @garyharrington5300 Год назад

    Never seen one before ,I shure appreciate belt driven accessories more

  • @4G63Tpower
    @4G63Tpower Год назад

    What’s the reasoning behind geared alternator? Are some busses belt drive? Hopefully the wireing gets all sorted when the new alt goes in.

  • @wirekat
    @wirekat Год назад

    So many McGyver's working on buses.

  • @donaldsayers4967
    @donaldsayers4967 Год назад

    I wonder if the electrical current flow due to the short might have caused damage to the bearing. I have seen the same type of things happen on motors that have low insulation resistance, current passes through the rotor back to earth through the bearings and basically ruins the surface of the bearings.

  • @sethtriggs
    @sethtriggs Год назад

    Yikes! Wow yeah that coulda even been worse indeed!

  • @Alanthe918mobilemechanic
    @Alanthe918mobilemechanic Год назад

    I think someone welded that fitting and hit the case with their chipping hammer tryna clean the slag off the weld.

  • @rickey5353
    @rickey5353 Год назад

    Performance evaluation: Can you climb "Monkey Mountain"?

  • @waynep343
    @waynep343 Год назад

    When you go to reassemble. Are you going to run the output cable. The relay and field wire thru at least a foot of fire sleeve or 1" heater hose.

  • @18robsmith
    @18robsmith Год назад

    A bunch of screaming cats in the engine bay - did he leave his wallet back there by mistake?

  • @fw1421
    @fw1421 Год назад

    That’s the biggest alternator I’ve ever seen! You deal with these vintage busses all the time. Is it common for owners to ignore routine maintenance? Knowing the age of these busses I would think owners would be more interested in the condition of their investment. Seeing the alternator wiring patched together like that would drive me nuts.

    • @BusGreaseMonkey
      @BusGreaseMonkey  Год назад +3

      There are so many items to maintain and it’s almost a full time job keeping up. Having that alternator replaced three years ago if should have been good for quite a while.

  • @lloydrobinson7081
    @lloydrobinson7081 Год назад

    keep the clips coming

  • @10intexas
    @10intexas Год назад +1

    Yes....a BGM video..

  • @frankchodacki6269
    @frankchodacki6269 Год назад

    MC-7? Very nice bus.

  • @mfc4591
    @mfc4591 Год назад

    If I am thinking right a taper roller bearing takes on side thrust way better than a ball bearing. Hopefully that ground up metal is in the filter. Thanks for the upload

  • @devinrogers6877
    @devinrogers6877 Год назад +1

    Glad this wasn't worse 😅

  • @hudsonvalleyrailandriverandair

    Propane welding stick?

  • @timf6916
    @timf6916 Год назад

    Good job

  • @nealdietz7063
    @nealdietz7063 Год назад +1

    Most common in that Location is a Cast Iron Bearing Housing that Bolts onto the Accessory Housing
    Inside is a Male Gear ⚙ that slips inside a female Gear ⚙ as a Connecter to the Gear train. On the outside is a Double V Pully that Belts run to the Alternator....

    • @BusGreaseMonkey
      @BusGreaseMonkey  Год назад

      When this bus was converted to an automatic they changed from a belt driven alternator to a gear driven one.

  • @hudsonvalleyrailandriverandair
    @hudsonvalleyrailandriverandair Год назад +2

    Good place for some loom lol

  • @MoraFermi
    @MoraFermi Год назад

    I'm surprised there's no shear pin anywhere between the engine and the alternator.

  • @wdavem
    @wdavem Год назад +3

    Could you please autopsy the rest of that alternator?

    • @wdavem
      @wdavem Год назад

      My guess is there's nothing beyond what you'd expect from an offset rotor. I'm only asking because it's a bus alternator /for interesting laughs.

  • @akawireguy1197
    @akawireguy1197 Год назад

    To me it looks like a high ampere current flowed through that brass fitting and into the aluminum case, or just the opposite. The brass fitting was better able to handle the heat from that high ampere current so the aluminum around it melted.

    • @BusGreaseMonkey
      @BusGreaseMonkey  Год назад +5

      What ever happened it’s probably good no one saw it or they might have pooped their pants.

  • @russchamberlain8755
    @russchamberlain8755 Год назад

    The ball barring moving created friction, the will draw energy to it. The wire short pulled the energy to the bearings. They got electric hot. The heat melted the contact location, look for pitting on the alt flange lip. The engine to alt will show ark pitting. Also.

  • @joseantoniocastrellonjr2568
    @joseantoniocastrellonjr2568 Год назад

    I bet it failed because the tapered roller bearing wasn't on the correct side.
    I bet that eroding happened because whomever installed it didn't disconnect the batteries before putting a wrench on it and grounded out on the case while hooking the power wire back up. 🤣

  • @bluebirdwanderlodgerenovat9715

    I have a new one in a box as a spare!

  • @iivaridark6850
    @iivaridark6850 Год назад

    Well, the wire looks smooth, not molten. Kind of would expect the heat melting the wire insulation... There is only abrasion marks and no signs of fire. If that starter aluminum housing melts it needs at least 900 Celsius grades. On the other end of the arc would be the wire and its insulation.
    Anyhow. Everything is possible. But it looks like someone tried to do some repair with something not suitable...

  • @awkwarddude
    @awkwarddude Год назад

    Geez, that alternator is the size of a small transmission!

  • @bryancooper2699
    @bryancooper2699 Год назад

    Is the battery door missing on the MC7?

  • @kevinvincent4323
    @kevinvincent4323 Год назад

    I’m assuming that since my seven has a generator still, I don’t have to worry about this problem. Correct me if I’m wrong. That bus would look a lot better if it had a red, blue stripe and a dog on the side.

    • @BusGreaseMonkey
      @BusGreaseMonkey  Год назад

      Even though your book calls it a generator it is in fact a 50dn alternator. But yours is most likely belt driven not direct gear drive.

    • @kevinvincent4323
      @kevinvincent4323 Год назад

      @@BusGreaseMonkey Yep mine is belt driven, but I did not know it was in fact a alt. Funny you said in the video that he did not have a not gen light. From what I've understood in the short time I've been a bus guy, is that having a not gen light illuminated is almost "normal" on Mci's of that time frame. Some of the guys on the bus monkey site said just turn on everything electrical you can and most the time it will put it out. Makes me wonder if it's getting an overvoltage. My light cycles on and off for a while then it stays on.

  • @ThisOldBus
    @ThisOldBus Год назад +1

    Is there was some sort of early warning situation for this type of failure? Besides just pulling it at 80-100k and having someone rebuild a perfectly good one and possibly screw it up for you? This is one area of concern on my bus I haven’t been able to address.

    • @Wayoutthere
      @Wayoutthere Год назад +2

      Being it a DUMB design for a start, I'd inspect it for wear (on the bearings). Seems like it's not that hard to remove, just heavy.

  • @bobbywright2100
    @bobbywright2100 Год назад

    Red looked freshly spliced to other wire??

    • @BusGreaseMonkey
      @BusGreaseMonkey  Год назад

      We pulled electrical tape off it to see how if was connected. It was old tape

  • @robp7652
    @robp7652 Год назад +2

    You said you think there would be a fuse. I’m betting the original red and black wire that was spliced had a fuse link in the wire and burned up previously. My guess anyway.

    • @Wayoutthere
      @Wayoutthere Год назад +2

      Yep, must be. 'Those annoying fuses keep blowing on me, gonna remove it.' etc.

    • @bus-fun-addict
      @bus-fun-addict Год назад +1

      As for the black and red being flip flopped at some point, some of the early regulators were set up to control the ground side of the field. It may have been switched to a regulator that controlled the positive side. The negative side regulators are not readily available anymore so most set ups have been converted to positive side control.

  • @AlCabin1
    @AlCabin1 Год назад

    Jb weld?

  • @gordoncorey8023
    @gordoncorey8023 Год назад

    Must have been on a side of the road fix on the wiring

  • @pinwizz69
    @pinwizz69 Год назад

    Looks to me like a very incompetent individual worked on the bus.
    In fact most likely 2 individuals.
    One that used a piece of red wire to replace some missing black wire twisted together and black taped and not secured correctly to avoid that short.
    Another that rebuilt that unit and installed the beerings incorrectly.
    From the look of the design ball beerings would be a really bad idea in that position even if they're sealed bearings.

  • @bobscott9253
    @bobscott9253 Год назад

    The mysterious Arc marks may have been from someone before removing the battery cable and touching it accidentally? Idk what I'm actually looking at. Lol

    • @BusGreaseMonkey
      @BusGreaseMonkey  Год назад +4

      The bus owner says those melted bits were not like that when the alternator went on.

    • @sledhead904
      @sledhead904 Год назад

      @@BusGreaseMonkey wow, had to be that shorted wire then! Crazy it wasn't enough to melt all the insulation off the wire. Would adding a fuse right off the ring terminal be benificial? Or just secure the wiring properly?

  • @1982MCI
    @1982MCI Год назад +1

    Hey Lance………… Ah no, not today, it’s now…… Hey Don!!! This is NOT the video I wanted to see right now!! Especially at 3am, cause now there’s absolutely no way I’m gonna get back to sleep at all!! This is the exact same problem I’ve got on my 82 MC9 with the 8V71. Yep, I did get
    ROOKED by the church, just like I thought.
    I just bought this bus and the entire day I was there looking it over, I started it 5-6 times and drove it a couple times, walked around it checking all the lights and they were burning good from what I could tell but it was still light out at the time. I did not have any warning lights on the dash for no-Gen, or anything else. The bus was running great, as it should for the engine only having 10k miles since rebuild but that was about ten years ago when it was done. I finalized the transaction and was giving things in the cockpit one more good looking over before I was gonna leave and I noticed the amp gauge on the dash was in the yellow and reading approximately 22amps which is extremely low for a 24 volt system so I said something to the church Deacon that I had been dealing with through out this entire process and I asked him again if they had been having any charging issues cause the amp meter was reading low and he once again stated that no, they had
    Not had any charging issues, had not had to ever charge the batteries at all unless they had forgotten to shut off the main battery disconnect, which is fairly common on these, but the lights seemed to be burning good, and it had started fine all day giving me no indication that the batteries were not charging and especially the fact that I did not have the “No-Gen” warning light illuminated on the dash panel. At this point, I was thinking that it was completely possible that I had a faulty gauge. I’m a. Old jet engine mechanic from the Air Force and that happened to gauges all the time and nothing e
    was indicating, without actually putting a meter on it to see what it was producing but since I flew to Florida to look at it , I was limited on what tools I had
    I made the decision, after being told by both the church Deacon, as well as the pastor himself, numerous times that the bus had just come out of a complete and thorough, top to bottom, inspection to be sure it was road ready and had no issues and was ready for a cross country trip except for the air conditioning. I made it about 40 miles down the road and I lost all lights cause it was apparent by now that I had generator issues.
    Long story short, I managed to limp her the 500 miles home by having to jump start her each morning, which for jumpstarts for three mornings I accrued $800 in jump fees which I feel like I got raped over but I had to get home. I have not torn into that part yet because I’ve been trying to research it to find ouT what the issue was cause the no-Gen light not being illuminated on the dash was throwing me off but this video pretty much explains it all right now.
    Scott, when you say this is an engine killer, what do you mean exactly? What other indications do I need to look for that I have bigger issues? I have not driven the bus since I got her home until I could figure out what’s happening. The oil looks good so far and I don’t have any screaming cats back there when I have started it a couple times. Is this simply gonna be a generator change or what am I looking at? I was gonna try and schedule a visit with you guys this summer when you could get me in an I am a patreon member but it sounds like this may be something a bit more critical than being able to wait if I’m in danger of trashing the engine. Please Scott, advise me what to do here brother! This video now has my stomach wrapped up in knots! But at least this explains my situation and what has happened, now I just need to know how to proceed.
    Thank you Scott for all you Kelli, and Tyler do to help us keep these buses on the road.

    • @BusGreaseMonkey
      @BusGreaseMonkey  Год назад +2

      The direct gear drive alternator can destroy an engine if they fail. Yours is maybe not gear driven but if it is not belt driven and it’s not working i would recommend finding out what’s wrong and inspecting the alternator. Usually a non working alternator is not to big of a deal to fix or get working.

    • @1982MCI
      @1982MCI Год назад

      @@BusGreaseMonkey the one on my engine tho scott is identical looking as the one you pulled off in this video. It is located on the very back left side of the engine and is directly below the access hole in the floor at the very back of the bus. It is not belt driven at all and is huge. I’ll call Luke today to see if he’s got one that matches it.
      Thanks Scott

    • @RealJoshMisner
      @RealJoshMisner Год назад +1

      I have a brand new 24v 50dn I will sell you at a discount to help you that will work for your girl

    • @BusGreaseMonkey
      @BusGreaseMonkey  Год назад +4

      Diagnose the issue before buying one. Check the voltage regulator.

    • @RealJoshMisner
      @RealJoshMisner Год назад +2

      @@BusGreaseMonkey I second that. They’re a lot easier to replace and cheaper as well. I’ve got a few.

  • @KuntalGhosh
    @KuntalGhosh Год назад

    Why is this alternator oil cooled?

    • @sidlori1592
      @sidlori1592 Год назад +3

      Well, from a strictly electrical perspective, the back section of the alternator has the six rectifier diodes that are wired up for a 3-phase AC -> DC conversion. (Visible in this video at 8:05...3 are up on top, going to the output wire; the other 3 bolt directly to the alternator frame.)
      The problem is that the 50DN alternator is rated for 270A. Rectifier diodes will easily drop 1.2v each (or more, depending on their spec!) at such currents...and due to the 3-phase rectifier method, power is always going through at least 2 diodes (positive and negative output). This means that at full load of 270A * 2.4v loss (1.2v per diode) = a happy 648W of heat dissipation in the back section of the alternator alone. (Yes, to be technical, this does get spread out evenly across the diodes on all 3 phases, so technically each diode has to dissipate ~108W.)
      I always like to compare heat dissipation to a soldering iron...a 25W soldering iron can melt solder. Imagine a similarly-sized diode being responsible for 4x that power: without oil cooling (or LARGE heatsinks!), these diodes will melt VERY quickly under load!

    • @MrHortoncoolstuff
      @MrHortoncoolstuff Год назад

      @@sidlori1592 The man knows his stuff. Believe me.

  • @coastalcowboyentertainment6284
    @coastalcowboyentertainment6284 7 месяцев назад

    Where are you fellas located I’d like to start using you for my repairs. I have a 1995 Prevost XL and a 2003 H3-45. Both always need something. If I could acquire a phone number and/or email with location I’d surely appreciate it. I’m worn out with repairing, driving and I just wanna do the singing from now on. Thank you
    GT

  • @RealJoshMisner
    @RealJoshMisner Год назад

    I’ve got a brand new 24v 50dn alternator for anyone who needs it for a great price to help out

    • @BusGreaseMonkey
      @BusGreaseMonkey  Год назад +1

      Josh helped us with parts on the eagle Christmas bus job recently. He’s real.

    • @RealJoshMisner
      @RealJoshMisner Год назад

      @@BusGreaseMonkey thank you so much brother!

  • @dannygoin6552
    @dannygoin6552 Год назад

    🇺🇸🇺🇸🇺🇸🥃🥃🥃☕️☕️☕️👀👀👀👍👍👍🍻🍻🍻🇺🇸🇺🇸🇺🇸

  • @Wayoutthere
    @Wayoutthere Год назад

    What a dumb design, same level as modern timing belt engines that can destroy the entire thing just from snapping a belt. How about a shear pin?? EDIT, just for some sick lulz, inspect the ball bearing for electrical arcing (pitting).