Fixing A Poulan Leaf Blower That Won't Start The Hard Way

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  • Опубликовано: 23 окт 2022
  • Links to products I have in my tool bag.
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    Above are affiliate links which means we receive a percentage of the revenue made from purchasing products via those links.
    Thanks for watching. We finally put this blower back together, and hopefully it starts, otherwise, it's going to cost me more money.
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Комментарии • 275

  • @butler386
    @butler386 Год назад +30

    I believe your idea of the stuck ring is spot on. Freeing up the ring also increased the compression by a bit more that two fold. I never thought of that being a problem. But will tuck that away in my top pocket. Thanks for the videos.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +2

      thank you D Butler, I appreciate your time.

    • @kaaraa-mardha1977
      @kaaraa-mardha1977 Год назад

      @@HomeGaragechannel Hi there , my primer bulb is sponge and hard to pump, what should I do? Also I sprayed starting fluid and still engine is not starting. My engine is 25cc craftsman leaf blower. I see spark, compression is 75 psi , still not starting

  • @vonclohk507
    @vonclohk507 7 месяцев назад +5

    Amazing. Man I wish there was a mechanic like you in my town.

  • @hillonwheels8838
    @hillonwheels8838 Год назад +6

    Seeing that the idle screw was all the way in is a sign that the blower has been having problems for a while. Great job getting it running again.

  • @robwebnoid5763
    @robwebnoid5763 Год назад +11

    Nice diagnosis. I'm just learning about small engines a little bit, so this stuff is news to me. I had recently fixed (about 3 months ago) my old gas string trimmer which I had not used in about 30 years. The worst part was just a crumbled fuel line which was a shock to me, but then it made sense since it was made of rubber & it's been 3 decades. Also replaced spark plug which I should not have had to, but the old plug rolled off the desk & broke in 2 on the ground, heh. Imagine that, a 30-year old spark plug was just minding its own business in a trimmer just sitting in the garage unused for 30 years & then some idiot human took it out & boom, it breaks after hibernating for 3 decades, heh. My trimmer is humming along nicely & I can now use it, especially when my electric trimmer is having issues with the line auto-feed mechanism.

  • @wapd205
    @wapd205 Год назад +8

    I’m learning more and more by watching your videos. I would’ve stopped after checking everything you did and given it back to the owner. Thanks for sharing the information.

  • @nelsonbrum8496
    @nelsonbrum8496 Год назад +5

    "They'd never be that greedy."
    Sarcasm detected! 😂

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +2

      in fact, the Sarcasm meter is pegged out, on this one. thank you Nelson Brum.

  • @garymucher4082
    @garymucher4082 Год назад +4

    I honestly believe those blowers were made to replace about each year or two. I've had a couple and never fails, they stop working after a season or two. However, I bought a Stihl blower (a few dollars more) and I have been using that for at least six years without and problems... Guaranteed it starts and never have to worry about it working!

  • @rickthelian2215
    @rickthelian2215 Год назад +3

    Wow that’s a big improvement to the Compression...
    Interesting story and my first stuck ring on video or live😊

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +2

      thanks, and yes the improvement was extremely impressive, thank you Rick Thelian.

  • @ricknicholson8698
    @ricknicholson8698 Год назад +3

    Great video. I have learned so much that I have purchased a 16 year old Troy Bilt mower to try my hand at small engine repairs. Thanks again for the indepth videos.

  • @angelon7095
    @angelon7095 Год назад +1

    I have the same blower. 2 years ago the piston ring was stuck and I did this same fix. It's been working great ever since.

  • @josephsfields
    @josephsfields Год назад +6

    Glad to see your success with this blower. I have one on the shelf of that same brand that probably needs the same treatment. Glad you went the full measure on diagnosing this one and showed the disassembly too.

  • @tedstankunas7142
    @tedstankunas7142 Год назад +4

    I work in a small engine repair shop, and we use Echo Red armor with good results in cleaning carbon buildup. Running one tank full through an engine makes a big difference..

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      really? is that something that's written in their claims? I'll have to take a look into it, thank you Ted Stankunas.

  • @dws2313
    @dws2313 Год назад

    Thank you for this series of videos. It helps me to troubleshoot my leaf blower problems.

  • @salsasamuri
    @salsasamuri 2 месяца назад

    This actually helped me to find out, that my Stihl that my dad left behind had 50psi of compression. It was over before it even began. 😮😅

  • @jamesazahn6842
    @jamesazahn6842 Год назад

    It's amazing as to how much I learn from your vedios,."Thanks", your knowledge is much appreciated!

  • @garyalensr
    @garyalensr Год назад +3

    You never cease to amaze me great job getting that going. I'm so glad I'm subbed to your channel. The amount I've learned a ton from you. Thank you

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      Thank you Gary Allen, I really appreciate the time you give to this channel and all the comments. It means a lot to me.

    • @garyalensr
      @garyalensr Год назад

      @@HomeGaragechannel Your very welcome!! Im so grateful you take the time to upload your knowledge for us. Like I said before, you explain everything perfectly. I've learned so much about Small engines from you. I just wish there was more I could do to show my appreciation.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      just keep watch, that's all I ask.

  • @therandomman6647
    @therandomman6647 Год назад +18

    How much compression the engine needs to start is dependant on how big the engine is, if 2 differently sized engines have the same size leak in pressure, the one with the bigger displacement has more air that needs to be leaked over the same period of time, so it can run on lower compression levels.

  • @deebee3901
    @deebee3901 Год назад +2

    Great blower and fantastic repair. I believe that the stuck piston ring caused too low compression and this combined with poor air and fuel flow caused this blower not to run.

  • @ezragonzalez8936
    @ezragonzalez8936 Год назад

    I have the same blower I have not baby it used ethanol fuel nor have I ever drained the fuel during winter in Utah and yet it has served me well for over 11 years now runs like a champ! cheers great repair!

  • @adamkubasik8706
    @adamkubasik8706 Месяц назад

    Thanks to this video I was able to take apart my poulan blower and the piston ring was also stuck, unfortunately it broke trying to get it off so I have 2 new ones coming , hopefully after installing that and changing out the gas lines as they were corroding it’ll work fingers crossed! Great videos I’m addicted! If you have a email I could send a question to I’d appreciate it as I’d be able to send a picture of what I’m talking about on another project I’m working on, thanks again for the awesome videos

  • @denisconor648
    @denisconor648 Год назад +2

    Great job.

  • @MikeJones-jr5hb
    @MikeJones-jr5hb Год назад

    I have also had a two cycle engine that had one seized ring the other wasn't. my model had two piston rings. i had to put my drill on it to get it to fire. Good video!

  • @majorpayne5289
    @majorpayne5289 Год назад +1

    👍Good job. I’ve NEVER seen this manufacturer start this easy. NEVER! 💩

  • @markharris4260
    @markharris4260 Год назад

    It sounds good now ! Yes carbon build up on the piston over time then one day you run it hard shut it down and as the piston cools off the ring gets stuck , it does happen more than you would think , great job on your repair work !

  • @Nukemann64
    @Nukemann64 Год назад

    Awesome repair IHG! I commend you on finding the issue and fixing it. I ROFL'ed at you saying "this blower is lucky to be $50 on a good day in November!"
    I'll try to remember that one!

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      thank you Jacob Feather, I'm glad you got the reference

  • @stevekurtenbach1951
    @stevekurtenbach1951 Год назад

    I have the same leaf blower and was having trouble with it running. All I did was change all the fuel lines. Fuel filter and put a after market carburetor from Ebay for $13.00 and adjust the it a little. Starts great and runs really well.

  • @Jim-ie6uf
    @Jim-ie6uf Год назад +1

    Well done!

  • @Turningwrenches85
    @Turningwrenches85 Год назад

    Very good diagnostic on this blower here

  • @jjjuarez312
    @jjjuarez312 Год назад

    Excellent Job there boss!! You did the right thing by taking it apart and rebuild it!! Sometimes a rich mixture of too much oil in the gas will cause it to burn rich making carbon disposits will gunk up engine internally!! Will also Sometimes score cylinderwall s and stuck rings on piston...

  • @andymaldonado3449
    @andymaldonado3449 Год назад

    That’s exactly what my blower is doing. Thank you

  • @Patrick4959
    @Patrick4959 Год назад +1

    from my view in this case mostly yes and of course i find keeping it good clean shape and of course doing some of the normal tasks will keep something like this running good and top notch too etc.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +2

      you are correct, thank you Patrick Stapleton.

    • @Patrick4959
      @Patrick4959 Год назад

      @@HomeGaragechannel for sure mate i keep mine clean and in good condition and doing yearly basics from replacement parts including fuel filter and fuel line changing and even the spark plugs and whatever it needs and it,s a dead easy one to start for me and i keep my repair bills down as best as possible unless it was out of my skills etc.

  • @anthonycorcella7300
    @anthonycorcella7300 Год назад +4

    Gotta love it! Now your family member can go back to annoying their neighbors every Saturday morning Oct-Nov. :D

  • @revelationhomestead1776
    @revelationhomestead1776 Год назад +1

    Success 🙌 🥇 amazing work

  • @baddad5781
    @baddad5781 8 месяцев назад

    Good one man as always

  • @jamescsolak9499
    @jamescsolak9499 20 дней назад

    That’s just what mine is doing, I guess I’m going to try to do exactly what you did!😊

  • @bertgrau3934
    @bertgrau3934 Год назад

    I have Poulan leaf blower to, was built in 2007 I just changed the carburetor, fuel lines, fuel filter, and air filter. I started it right up, no problems, I did make small adjustments to the carburetor.
    The fuel lines had broke, years ago. And it sat for at least 9 or 10 years. It cost me less than $20 to fix, and I can sell it for around $50-$60 . I can use it as well.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      nice, these do have some value in them, thank you Bert Grau!

  • @Franklinveterinarycenter1of4
    @Franklinveterinarycenter1of4 Год назад

    Wow! Love your channel.

  • @LeoThePool
    @LeoThePool Год назад

    I bought a blower like this except it's a craftsman for 20 bucks and it just needed the idle screw adjusted. I think it's pretty reliable and a good replacement for my homelite tank.

  • @patthesoundguy
    @patthesoundguy Год назад

    Obviously the stuck ring was the issue. Another one saved 👍👍👍 I also really like the idea of the extra hole in the exhaust. You actually could make it match the original outlet if you wanted to without issue. The extra flow helps get rid of heat from the engine, and as long as you adjust the carb to compensate for the extra flow it will be fine. That stick ring was definitely from too oil by the looks of what was in the tank, if the blower wasn't run much up at full operating temperature, it would have a hard time burning the excessive oil off. Also if the exhaust was a little plugged up with carbon like you thought it would be running richer than normal, making the problem worse. Great repair as always 👍👍👍👍

  • @loborobertson7212
    @loborobertson7212 Год назад

    Super good video and good job 👍👍🤠

  • @aeson33
    @aeson33 Год назад +1

    First time my cylinder bolts backed out it sounded like a crotch rocket. Second time I put the thread locker on that the factory forgot. It is a flaw, you are correct.

  • @electroddxful
    @electroddxful Год назад +2

    Great video 👍🙏👍🙏

  • @Ron0963
    @Ron0963 Год назад +1

    Nice job! ..I was right on how many pulls to fire it up. a buddy has that same blower

  • @Skyliner_369
    @Skyliner_369 Год назад +2

    It could be that as the carbon was building up, the ring, piston, and all were hot, and so, everything was fitting perfectly as it ran, and as it cooled down, it shrank, pulling the seals away from the walls, making a massive gap. Also I think you're right about the lack of fuel draw.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      oh you make a good point!

    • @cadewey6181
      @cadewey6181 Год назад

      . . . Along with a fill up of too oil rich fuel in cold engine. Great video

  • @wildefox1478
    @wildefox1478 Год назад +1

    Great video, I believe the stuck ring was the reason it wouldn't run, 2 strokes won't run if they're low on compression. They probably either used a cheap low quality oil in the gas or they added too much oil causing the piston ring to become carboned up and stuck.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      thank you WildeFox, I also believe the quality of the oil and gasoline, has a huge impact.

  • @jct300m
    @jct300m Год назад

    Nice job!!!!!

  • @paulkonczak5270
    @paulkonczak5270 Год назад +2

    Yes I think stuck ring was the cause. I’ve had two units with a similar problem. Poulenc pro ran like crazy then the next day wouldn’t start. Turned out one of the cheaply designed engine 2 screw cylinder bolts snapped. Sad when the only use 2 bolts to secure the the cylinder to the block. Tried drilling it out with no luck so it’s junk. Bought a Echo 2620 with 4 bolts and bearings on both sides of the crank. Not that much more$ but it’s a pro model and should last. The other unit was a craftsman, turned out ignition module too far from flywheel, regapped and starts with 1 or 2 pulled every time.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      you definitely made a good choice, in buying the echo, thank you Paul Konczak.

  • @Furrowx
    @Furrowx Год назад

    Excellent You were spot on about the stuck ring!
    What is Your go to Or favorite Mixing oil brand?

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      thanks, and I don't have a favorite, just the cheapest one on the shelf.

  • @TheDronzDr
    @TheDronzDr Год назад

    You are correct

  • @TecumsehRulesbcserk
    @TecumsehRulesbcserk Год назад +4

    It’d probably be best to use the premixed engineered fuel for this thing since it tends to not produce as much carbon. Unless you are daring enough to run 60:1 in this thing.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      yes you are correct, the engineered fuel would make a lot less carbon.

  • @alexs2778
    @alexs2778 5 месяцев назад

    Just had to fix one that my smart brother gave to me. It was very hard to start and once started the revs were inconsistent even when warmed up. Checked the ring and it had some build up but not enough to make it stuck. The culprit was one of the 2 screws that holds top of the engine to the bottom, it was loose, after cleaning and reassembly you could feel just by pulling rope that it had more resistance to it and it started right away and run like new.

  • @RealWickedAlliance
    @RealWickedAlliance Год назад +1

    Looks like you saved them alot of money.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +2

      quite possible, I would have suggested in buying a good used blower instead, like an echo or stihl.

    • @RealWickedAlliance
      @RealWickedAlliance Год назад

      @@HomeGaragechannel I have a 4 stroke craftsman back pack blower I got for cheap any thoughts?

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      sure, I would check the valve lash because it's recommended it be checked once in awhile

  • @gilpicard6024
    @gilpicard6024 Год назад

    Cheap fix just replace the rings and off you go , there out to make money like ever thing else. Good vid as usual , thx

  • @RussellBooth1977
    @RussellBooth1977 Год назад

    Yes I do believe that the stuck ring caused the engine not to start,I am glad that I rekitted a Stihl hedge trimmer with a new cylinder kit when I couldn't get the reading above 75 PSI although it also had a shot ignition coil.
    The reading was then 105 PSI then 120 PSI once the engine was run in.
    It's unless it's like my L headed Briggs and Stratton powered lawnmower where it has a 6:1 compression ratio & they recommend giving it a cylinder leak down test because a compression test won't give a true reading that I will perform a compression test.
    As far as using threadlocker on the cylinder bolts,the Stihl hedge trimmer engine had self tapping screws fitted so I had to tap them out oversized & fit bigger screws in the new aftermarket cylinder kit because they wouldn't fit & they strip out at the best of times once undone & even with the original parts !

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      yes you are correct about the leak down test. Thank you Russell Booth.

  • @WhiskeyGulf71
    @WhiskeyGulf71 Год назад

    I’m pretty sure you can make this repair without disassembly, by pouring neat gas in to the cylinder whilst at tdc through the sparkplug hole & letting it sit for a while.
    As a side note, i run all my equipment on pump gas which is 10% ethanol & a cheap 2S oil, never have any problems but i do always purge the fuel out when i’m not planning on using them within a week or more.
    My oldest unbranded & well used blower is now 5 years old & i have just fixed a poor starting issue by stripping, cleaning & rebuilding the carburettor with new gaskets a new metering diaphragm, i don’t think the old diaphragm was bad though, i just had a new one to hand.

  • @bleach_drink_me
    @bleach_drink_me Год назад

    My brother has had one of these for years. He only uses canned fuel or ethanol free 90oct with synthetic 2 stoke oil.
    He always runs it out of fuel before storing it for the winter. His still starts and runs like new.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      I like the way, he's taking care of it, thank you for sharing.

  • @sparky1044
    @sparky1044 Год назад

    That piston was gummed up almost as bad as the transfer pump I was telling you about. Wow!

  • @TargaWheels
    @TargaWheels Год назад +3

    Compression on a 2-cycle is more critical than a 4-cycle. There's no way to change it externally except with a compression release (relief) on some engines. When it fires and goes down, not only is it exhausting out the exhaust port, its taking in through through the slots in the cylinder on the way up. When that piston ring passes the slots until it tops out in the cylinder, that's all the compression its going to get. Crazy how the compression can get that high, but it takes a lot of cycles to do it.

  • @gordrobinson4780
    @gordrobinson4780 4 месяца назад

    My ring does not have rectangular cross section. One side is chamfered toward the outer edge. I assumed that was to make it easer to get back int the cylinder. But that could lead to a compression leak. I could not see if that was how you oriented the ring in your video even with it slowed down. BTW your videos and commentary are superb and I really appreciate your reply to my comment.

    • @HomeGaragechannel
      @HomeGaragechannel  4 месяца назад

      thanks, and I'm using the chamfered end of the ring to align the ring. There's no chamfered edge on the ring I re-used.

  • @joesphbaumgardner4579
    @joesphbaumgardner4579 Год назад

    Agree these are good blowers vs some garbage blowers now. That is, when they work lol. I worked mowing lawns for years long ago with a 85 year old man. He had a Craftsman same style and look as the Poulan. Said he brought it new long ago. Put nothing but no eth gas in it and Stihl oil. What I do know is it ran without a issue and still does. At the time I wanted one and had no blower. Course they are old and finding one is a hit and miss. Speed up to some years and I seen the Poulan on market place for 20 bucks. Brought it and of course carb issue. I must of been inside that blower and carb dozen times. Got it to run and still does, but prob needs new carb. Then out the blue I seen them and the black older Craftsman blowers that look like yours in vid. Story is, now I have about a dozen Poulan yellow and 5 so Craftsman just like it. Now that is not to say they been a pain as in working on. That is because knuckle heads prob used them prior and now issue after issue. I learned alot of time can be wasted in these blowers. A pain to strip down and better pay attention how all goes like that throttle spring under handle lol. I robbed peter to pay paul on a few. Rest is parts but 3 I just put to side long ago. In that 1 you pull the cord and it is so sloppy and no pull back ( ? compression, junk it? ). Other one I just can't get started after carb clean many times and rebuild in parts. I have not checked the ring. Truth be told I never did on any of them. I always thought one needed some tool or something and skill before messing with a ring. I see maybe not in vid as you got all right on and back in without tool. I will say I find the blowers have mood swings. They can run great one day and next darn thing won't start. I use my Craftsman just like that Poulan I rebuilt carb on and it fusses some but few years and still goes. Course I use 90 no eth and Stihl oil. What I can't oddly still get is a part number on that Poulan carb. I searched high and low and asked around. What is the carb part number? Good vid.... Yes, I seen a few where the bolts for engine block get play and back out. I recall right on that Poulan I think one bolt is a pain to get at. Thread locker or JB weld.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      yes you are correct, these blowers have moods and sometimes it a no go, with them.

  • @byzon123
    @byzon123 Год назад

    Hey great vids wondering whats that spray you use to clean the engines seems to work great on removing the grime and oil

  • @crazzywolfie
    @crazzywolfie Год назад

    had someone give me one of these today. hopefully it is not that much of a pain to get running.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      good luck to you

    • @crazzywolfie
      @crazzywolfie Год назад

      @@HomeGaragechannel finally got to look at it and likely has the same issue or possibly worse. compression test only showed 40psi even tho the cylinder doesn't look too bad inside. not sure i will bother fixing it despite it looking in very good shape. really doesn't seem like it will be worth fixing if it is a common issue.

  • @williamsnow1531
    @williamsnow1531 Год назад

    It sure does sound believable to me. You just proved it.

  • @garyamaral9905
    @garyamaral9905 9 месяцев назад

    Hey love ur vids!! I have a poulan pro leaf blower like vid. But with one carbarator it stay running without holding throttle. Bought another new one and doesn't stay running unless holding down throttle. And I have Tryed to adjust the carbarator.
    Any thoughts please?
    Thanks

    • @HomeGaragechannel
      @HomeGaragechannel  9 месяцев назад

      when you say adjusting the carb, were you turning the fuel adjustment screws are the idle set screw?

  • @lewiemcneely9143
    @lewiemcneely9143 Год назад

    Sure the ring is believable, along with planned obsolescence! The outfit ai was working for doing lawn maintenance had got a new batch of Snapper walk mowers but with Tecumseh 2-cycle engines. None would run right the 2nd season where the Briggs I/C 2-cycles lasted for years. The compression in the Tecumseh's was GONE! Can't remember if it was a fix of new mowers or just ew mowers with good engines. You did GOOD and Blessings!

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      wow, the difference between the engines is quite amazing. I wonder what happened to it?

    • @lewiemcneely9143
      @lewiemcneely9143 Год назад

      @@HomeGaragechannel These mowers were run as in commercially. The Briggs with the cast iron sleeve and Stihl oil could take it. everything was walk mowed. The Tecumseh mowers were fed the same mix of Stihl oil but just couldn't take the constant running. I mowed one yard by myself every 2 weeks that took 7 1/2 hours of steady walking except to fill up with gas and eat. That takes a toll.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      thank you, for the information

    • @lewiemcneely9143
      @lewiemcneely9143 Год назад

      @@HomeGaragechannel I try. All I can say anything about is what these old bloodshot eyeballs have been in the middle of.

  • @apatterson8128
    @apatterson8128 Год назад +1

    It was probably was hard to start before this, but the owner didn't know the signs of a stuck ring. Nice repair and thanks for teaching us how you diagnosed it. Did you tell him/her to ease up on the oil in the mix?

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      It wouldn't do any good. don't worry, I probably see it again next year for a different problem

    • @apatterson8128
      @apatterson8128 Год назад

      @@HomeGaragechannel That’s true. Lol

  • @pyrokamileon
    @pyrokamileon Год назад

    there is a link in this video's description going back to the part 1 of this story. but when I watched the part 1 of the story I checked its description for a link to part 2. I guess I might not be able to expect that kind of future proofing because the part 2 video hadn't been released yet but wouldn't old video descriptions be editable after the fact? either way I'm glad that my RUclips feed eventually recommended this video because I was curious about the follow up but I just wanted to let you know

  • @jerrysoutherland662
    @jerrysoutherland662 Год назад

    I got my 2 cycle manual over 20 years ago it said for any 2cycle engine to run right it needed 90lbs. compression are better to run right.

  • @lemmingeddie3045
    @lemmingeddie3045 Год назад

    I have a poulan pro blower i start it cold but after its been running its so hard to get back started most the time i have let it set a while i ajusted the carb new gas cap checked exaust not cloged but when it runs its strong ???kinda stumped ty

  • @user-gx7rr9mh9l
    @user-gx7rr9mh9l 3 месяца назад

    Thank you for this video. I have a Poulan SM400 blower, and it's very oily and dirty. I noticed you cleaned it and easily used water to wash it. 0:50 Can I also use water? I wanted to try, but I'm concerned about damaging the carburetor, engine, or something similar.

    • @HomeGaragechannel
      @HomeGaragechannel  3 месяца назад +1

      yes you can, just so long as you keep from spraying directly into the carb, or muffler

  • @tiredoldmechanic1791
    @tiredoldmechanic1791 Год назад +1

    The problem with the stuck ring isn't so much the lack of compression but the failure of the piston to create a vacuum in the crankcase on the upstroke to draw the air/fuel mixture in through the carburetor.

  • @Cinder2008
    @Cinder2008 Год назад +1

    Could the stuck ring been the result of not running the engine wide open?
    I’ve heard 2 strokes were made to run wide open.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      there's a good possibility , but without watching them use it, it's only a guess.

  • @zeke112964
    @zeke112964 Год назад

    Had the same thing happen to mine Poulan BVM200

  • @mikehannan8932
    @mikehannan8932 2 месяца назад

    Are there any solvents or fuel treatments to keep the ring floating and un seized ? I use enthanol free gas synthetic 2 stroke oil. Thanks.

    • @HomeGaragechannel
      @HomeGaragechannel  2 месяца назад

      no, you just have to let the engine "cool down" before you turn it off. Also don't let the engine idle make sure that you have it running at full speed, after it warms up.

  • @anthonycorcella7300
    @anthonycorcella7300 Год назад +1

    I see a link to the chemical bottle, but what is the magic cleaner you use that works so well?

  • @gordrobinson4780
    @gordrobinson4780 4 месяца назад

    Is it possible to install the piston ring upside down? I could not get the piston back in until I turned the ring over so the side with a chamfer was on top then it slipped in. But now the compression is only 90 psi. Do I need to turn the ring over and try to get it into the cylinder?

    • @HomeGaragechannel
      @HomeGaragechannel  4 месяца назад

      on this piston , you the ring can only go one way as shown in the video. Did you install it like the way it was shown?

  • @lucascovitz5708
    @lucascovitz5708 3 месяца назад

    Any idea if the spark arrestor screen on these particular blowers can be cleaned? I had the muffler off of mine today, and it looks like it is welded together and can't be taken apart to do so. Would like to take a look at the screen and clean it if needed, as it hasn't been done in the almost 10 years since I got it.

    • @HomeGaragechannel
      @HomeGaragechannel  3 месяца назад

      no the screens in these cannot be easily serviced, you'd have to put the muffler into a fire pit

    • @lucascovitz5708
      @lucascovitz5708 3 месяца назад

      @@HomeGaragechannel Thanks for your help.

  • @46tool25
    @46tool25 Год назад

    Hey HG, what are your thoughts on Honda exiting the lawn mower market and discontinuing the production of lawn mowers by 2023

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      hmm.. it's a smart move. They want to focus on all the other things they've got going on, which is a lot, and let the cheap overseas "stuff" flood our market. it makes sense to me.

  • @kylec.3259
    @kylec.3259 Год назад

    Just a thought here from a shop tech. Primary vs secondary compression. Hard to expain. Easier to google.

  • @robertmailhos8159
    @robertmailhos8159 Год назад +1

    The.proper oil to gas mixture is the most important thing to do

  • @nathenleffert_official
    @nathenleffert_official Год назад +1

    Yep definitely the issue with mine lol same exact one

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +2

      it happens a lot

    • @nathenleffert_official
      @nathenleffert_official Год назад

      @@HomeGaragechannel I got mine free used it once and acting like it's running really rich, I prime it with fuel disconnect the fuel line and runs ok ish but when you put the line back in it kills it immediately 5 seconds after

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      interesting, does the purge bulb cycle fuel?

    • @nathenleffert_official
      @nathenleffert_official Год назад

      @@HomeGaragechannel yea, carb is in excellent condition, primer bulb cycles, picks up, and returns

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      okay, would consider adjusting the carb, or replace it.

  • @scottfirman
    @scottfirman Год назад

    generally I have seen rings stuck more from sitting for long periods of time. The oil gas mix turned to goo over time and glues the ring back so the compression is lower than normal. Taking the exaust off and checking the cylinder for damage usually tells me if the engine is worth fixing or not. a clean cylinder and stuck ring seldom happends for me. Usually the cylinder is badly damaged. I use recreational fuel in all my equipment.

  • @marshallcollins3376
    @marshallcollins3376 Год назад +1

    Where do you set the ring gap when you don’t have a mark on the piston?

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      easy, we don't set the ring gap, at least not on this particular engine. there's only a pin, that locates the ring, to the piston

    • @marshallcollins3376
      @marshallcollins3376 Год назад

      @@HomeGaragechannel sorry for my inaccurate question HG. I should have said where to position the gap in the ring around the circumference of the piston if there isn’t a mark on the piston. I have seen several opinions including “it doesn’t matter, opposite either connecting rod pin, to in line with the exhaust port”.

  • @henryssmallenginerepair6332
    @henryssmallenginerepair6332 Год назад +1

    would you be ablle to tell us what cleaner you use to clean your tools and engines?
    i use simply green but it doesnt seem to do as good of a job as in your videos

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      sure, and yes simple green is good, but it's not has good as the Degreaser I'm using, from harbor freight. It's the best stuff, I've every used at least, up to this point. Thank you Henry's Small Engine Repair.

  • @emilioorozco8870
    @emilioorozco8870 3 месяца назад

    Hello, I have 2 questions and my questions are how do you know how much compression an engine is supposed to produce based of a PSI reading? And How can you tell from a PSI reading if the engine condition is good or bad?

    • @HomeGaragechannel
      @HomeGaragechannel  3 месяца назад

      as a general rule, for all small engines like this one, I would like to see a reading well over 135 PSI, and as for the second question, I'd say it was based on all the testing I've done, when I've tested them and they were "lower" 135, it just means it has some wear based on what I've seen. 135 and up, the rings and cylinder looked good, when they weren't the number was less, and when the rings and cylinder were scored, they reading was terribly low, say, 80 PSI.

  • @MrRmh3481
    @MrRmh3481 Год назад

    The B&S J19 plug is too hot. CJ6 is what it needs. Could this have been your problem?

  • @ericrichardson3332
    @ericrichardson3332 Год назад

    I bet they adjusted the idle screw when it started to run inefficiently and slowing down / bogging down doe to the piston ring getting stuck and the increased idle allowed unburned fuel and oil the sit in the combustion chamber making the oil in the cylinder to get thick and sticky and when it ran it burned the fuel but didn't get rid of the thick oil not all of it and made it worse that's my guess, only way to know for sure is to take the fuel that they used and pure some in a container that is open to the air but safe from water and let it sit for a while to see if it becomes sticky and oily / thickens like a syrup if so then the fuel most likely get left in the cylinder and didn't burn but the fuel evaporated and left the oil behind and it burned partially turning it black and sticky

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      yes you are correct, most often, someone will make that adjustment to deal with issues they're having. It's very telling.

    • @ericrichardson3332
      @ericrichardson3332 Год назад

      @@HomeGaragechannel yes I am guilty of doing the same thing but nowadays I try to fix the issues causing the problem unless I am in a hurry and don't have time then it may get postponed until a later date but I'm sure most of us have done similar things in the past also I just want to say a little knowledge about things such as this goes a long way and helps others understand why , how , where and sometimes gives them the confidence to repair their own equipment keep up the great videos and interactions with your viewers 👍

  • @BlakeEyers
    @BlakeEyers Год назад

    i have this blower and the newer style of poulan pro blower that is black and both of them will start up just fine and rev up good but when i release the throttle even when the engine has warmed up they both shut off about 5 seconds after i release the throttle and they just started doing this. i dont know why because the week before they both ran and idled great. do you have any suggestions?

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      did you add new fuel recently?

    • @BlakeEyers
      @BlakeEyers Год назад

      @@HomeGaragechannel yes i mix my 2 cycle fuel by the gallon.

    • @BlakeEyers
      @BlakeEyers Год назад

      @@HomeGaragechannel i have replaced the ignition coil and piston ring on one of the 2 blowers about a year ago but i think there is a carberator problem. i usually run seafoam through every tank of gas so thats very suprising that it will start but it wont idle

    • @BlakeEyers
      @BlakeEyers Год назад

      @@HomeGaragechannel and about 2 weeks ago it was idling perfectly.

    • @BlakeEyers
      @BlakeEyers Год назад

      @@HomeGaragechannel i am considering taking apart the carberator and cleaning it or just ordering a new carberator from amazon

  • @brennanschuler2155
    @brennanschuler2155 Год назад

    If I had to come up with a theory, I’d say the day prior, the engine was good and hot. User probably ran it all day and it was fine. The carbon and oil probably mixed good, and overnight it cooled off. Causing the oil/carbon mix to get gummy and solidify. Thus the ring got stuck. But I tend to overthink things.

  • @mikespain8655
    @mikespain8655 Год назад

    People that say put in a new carburetor, ignition coil, etc. are parts changers. They don't diagnose equipment, they fire the parts cannon until it is fixed.

  • @davidrawlings880
    @davidrawlings880 Год назад

    What cleaners do you use

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      I use a degreaser from harbor freight for the oily and greasy spot and LA Awesome cleaner for dirt.

    • @davidrawlings880
      @davidrawlings880 Год назад

      @@HomeGaragechannel thank you very much for te most part things just seem to come off fairly easy in your videos so thank you for the information

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      it's not for the lack of trying that's for sure.

  • @mr1pearl
    @mr1pearl Год назад

    Maybe it sat on the shelf a bit too long 🤷 runs great now 👍

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      that was my guess too but doesn't jive with the story I was told, oh well, works now.

  • @claytonpowell5855
    @claytonpowell5855 Год назад

    I have the same blower, however my issue is that it cuts out whenever you try to give it gas. I put new carb on it, new gas lines, gas filter. Blower starts easily but when given gas it stalls out.
    Any suggestions 🤔

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      oh you need to drill a hole in your muffler to help the exhaust get past the clog in your spark arrestor screen.

    • @claytonpowell5855
      @claytonpowell5855 Год назад

      @@HomeGaragechannel I tried drilling hole in muffler but made no difference, any other suggestions

    • @edwardgoodwin1813
      @edwardgoodwin1813 Год назад

      Try adjusting the High and low screws for the air mixture

    • @edwardgoodwin1813
      @edwardgoodwin1813 Год назад

      On the carburetor

    • @claytonpowell5855
      @claytonpowell5855 Год назад

      @@edwardgoodwin1813 I did and it runs well until I give it gas. Then it stalls

  • @MazichMusic
    @MazichMusic Год назад +1

    Poulan made a lot of Craftsman blowers back in the day when there were Sears stores all over. Today's Craftsman?

  • @danielpadgett2831
    @danielpadgett2831 Год назад +1

    I might be wrong but it looked like some carbon was built up in the exhaust port I was just wondering

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +2

      yes you were correct, I didn't clean it, but to be honest, it wasn't that bad.

    • @danielpadgett2831
      @danielpadgett2831 Год назад +1

      @@HomeGaragechannel I definitely understand that man that thing was alot of work and time glad you got it going thank you for all the new videos I also just got done watching the one on the populan chainsaw

    • @adamorsini4585
      @adamorsini4585 Год назад +1

      Drilling the hole in the muffler is giving it a performance mod. That should add 5-10 horsepower!

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +1

      thank you Daniel Padgett, I appreciate it!

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад +3

      lol.. I've got a few "racing" sticker, I can put on it too.

  • @NerfCraft
    @NerfCraft Год назад

    Clearly the stuck ring did impact compression. I think to say that it was unable to draw enough air/fuel to get the engine to start may be plausible, however you did put fuel straight into the spark plug hole, so if anything the only thing it wouldn't have been able to draw in that it needed would be air. Did the stuck piston ring actually stop it from sucking in air, I honestly don't know. In my opinion, I think this engine really does just require more compression in order to burn the fuel.
    As for the sudden failure, given that their oil/fuel mixture is a bit rich in oil, it's quite possible that the last run was just enough to finish seizing the ring. Also, once it was running the ring probably expanded a bit as it heated up, allowing the engine to maintain enough compression to just about stay running when they used it, but once the engine cooled, the ring would have shrank back down and no longer been able to build enough compression to run again. I've heard of this problem being able to happen with nitro engines for RC trucks. They don't even have rings, just relies on the fitment between the piston and sleeve to build compression. If your engine gets too hot, the piston will expand enough to enlarge the sleeve, but once it cools the piston and sleeve are too loose to create enough compression to start. Heat it up enough, it may be able to start again, but the engine would have to be running way too hot, and essentially it'll ruin the engine. And again, not knowing how it ran last time they used it, may have been running poorly. Could have had low compression causing the engine to have lazy performance, but if the owner isn't mechanically inclined or familiar with engines, they probably wouldn't have even noticed how poorly it was really running. They'll probably be amazed how smooth and powerful it is when you give it back.

    • @HomeGaragechannel
      @HomeGaragechannel  Год назад

      I hope so, it was quite telling when I found out they were running it at wide open throttle, so who knows how they were taking care of it.

  • @10forthebigguy753
    @10forthebigguy753 Год назад

    Echo red armor premium two-stroke oil clean carbon out of a carboned Up engine. It cost a little bit more

  • @jwayne777
    @jwayne777 11 месяцев назад

    Great video. Im wondering what chemicals or/ and tools you used to clean the piston, piston ring, and the cylinder chamber?

    • @HomeGaragechannel
      @HomeGaragechannel  11 месяцев назад +1

      is use carb cleaner, and a scotchbrite pad, and sometimes a small flathead to scrape it.

    • @jwayne777
      @jwayne777 11 месяцев назад

      @@HomeGaragechannel Thank you.

    • @HomeGaragechannel
      @HomeGaragechannel  11 месяцев назад

      no problem

    • @jwayne777
      @jwayne777 11 месяцев назад

      @@HomeGaragechannel so, i used this video to troubleshoot a similar blower and it turned out the flywheel key was sheared. I will be trying the polishing compound method on the shaft and flywheel method. I will let you know if it worked. An old motorcycle guru told me not to buy a $20 replacement flywheel because the problem would come back . He said use the rubbing compound trick first and keep the old flywheel

    • @HomeGaragechannel
      @HomeGaragechannel  11 месяцев назад +1

      it's worth a shot but what I do is to cut my own key way into the flywheel and install my own key

  • @eyeopener1993
    @eyeopener1993 Год назад

    to much compression is bad on an engine it causes pre ignition meaning the psi is reached to combust the fuel before the actual engine reaches tdc to spark. that's why there's always a sweet spot.

  • @hunter1953
    @hunter1953 Год назад

    The stuck ring was defenetely the problem. The problem with running one day and not the the other is simple did you ever run your car ever day and one morning the battery is dead that's just the way stuff works .