Mazdaspeed 3 Blows Engine On The Dyno After Making 400 WHP

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  • Опубликовано: 17 авг 2019
  • Unfortunately we blew the stock engine in the Mazdaspeed 3 on the dyno. All the tuning was done by me, and many would agree that it was not overly aggressive. It's hard to say what caused the failure at this point, but we noticed knock retard values above 5 degrees in the data log right before it let go. This didn't really make sense as we were running 94 octane pump gas mixed with 3 gallons of in tank methanol. The next possibility in our minds, is that using the WOT box as a rev limiter while making this much power and generating this much heat with back to back runs, might have stressed the engines stock internals to a point of no return. We already know that the OEM pistons and connecting rods are the weak points of this engine. At this point we've sourced another used CX7 long block and are going get it built with forged connecting rods, pistons, upgraded bearings, and possibly some head work. Enjoy the video! Please like, share, and subscribe :)
    Instagram - @wannabe_tuners
    Merch - teespring.com/stores/wannabet...
    Mods in this video:
    1. DM PCV Plate w/ Dual Vented Cans
    2. Cobb Accessport V3 (self tuned)
    3. Aeromotive 325 LPH Fuel Pump
    4. Bfg G-force Comp 2 All Seasons
    5. Stratified Guardian Angel V3
    6. Full Race Exhaust Manifold
    7. Ngk One Step Colder Plugs
    8. 6th Port Aux Fuel Injection
    9. Corksport Intake Manifold
    10. Jbr 88a Rear Motor Mount
    11. Jbr 88a Trans Motor Mount
    12. Jbr 80a Pass Motor Mount
    13. Custom Radiator Ducting
    14. Autotech HPFP Internals
    15. Eibach Lowering Springs
    16. Corksport Injector Seals
    17. Jbr Egr Block Off Plate
    18. Cpe Catless Downpipe
    19. Cfm Oil Breather Cap
    20. Jbr Raider's Air Damn
    21. MST Suzuka Wheels
    22. Koni Yellow Shocks
    23. Gen 2 Valve Cover
    24. CS 3.5 Inch Intake
    25. Cobb 3 Port Ebcs
    26. Fidanza Flywheel
    27. Bnr S4 V3 Turbo
    28. Jbr Under Route
    29. Cobb Xle Bpv
    30. AEM Gauges
    31. Cnt Catback
    32. Tr8 Fmic
    33. Wot Box
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Комментарии • 292

  • @sentryeldefiant7569
    @sentryeldefiant7569 4 года назад +39

    Dam that sucks, on the bright side definitely more content for the channel. Just hate to see it happen this way.

  • @JeromyGreen
    @JeromyGreen 4 года назад +19

    Oh my god my heart broke when that happened.

    • @WannabeTuners
      @WannabeTuners  4 года назад

      So did mine! Followed by a deep realization of "time to build" lol

  • @paulholmes3446
    @paulholmes3446 4 года назад +2

    Hope you get it back on the road soon mate. That's just savage. Great channel

  • @craigzilla100
    @craigzilla100 4 года назад +2

    Damn!! It's been a fun ride with the white speed 3.. sorry to hear, but also looking forward to seeing you guys tear it down and rebuilding.

  • @jasonc2948
    @jasonc2948 4 года назад +2

    Sad to see the beast blow on the Dyno. I've got a BL MPS that I blew the stock engine on, built it and loving it. Good luck with the build!

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      Thanks a lot! Wasn't expecting it to blow, but then again, do we ever?

  • @kimhongsoon6081
    @kimhongsoon6081 4 года назад +2

    Solid 400WHP with torque kept low and safe. Still it blew, that's unfortunate. Keep it strong mate, hope to see more videos on rebuilt process.

  • @pray4mysynths
    @pray4mysynths 4 года назад +3

    And I'm over here complaining about fuel pressure issues. All the best man!

  • @CHUDHUCKER
    @CHUDHUCKER 4 года назад +1

    Buggery, that sucks. I feel yer pain, I've been there 3 times, blown engines suck (not my 2008 Mazdaspeed3 yet). Never on a dyno either, always far from home!!!
    Would be interesting to see what went wrong as it seemed to be a hauntingly similar situation like Low Speed Pre-Ignition. Lex did a good write up about it on the forum. I used to work with him many years ago (before Stratified Automotive Controls) and can't even begin tell you how super detailed he is with the work he does. I remember him bringing in a bent rod (piston still attached) to work back in 2009 as he was trying to figure out what was going on with these engines. I used to do engine teardown/machining/building and the part he brought in was quite mysterious as it didn't have any of the witness marks associated with known failure analysis, anyways, I could see that he couldn't let this slide by. So maybe a chat with him about the tune could shed some light?
    Oh, I also feel your pain on the cost as I live near Vancouver, we Canadians pay 30-40% more for this hobby as the US has all the good stuff.
    Good luck to you.

  • @bionicnightmare6546
    @bionicnightmare6546 4 года назад +2

    I turboed my Mazda 3 hatchback with the 2.3 na engine and running 8lbs boost with no time currently I see you actually got another block so I'll just build my second block and swap engines when fully built internals, I've been watching your videos alot lately as I was installing the turbo on my car after the engine is built in going to add the meth then go for a bigger turbo

    • @amberheardslawyerprofessor5266
      @amberheardslawyerprofessor5266 4 года назад

      Yeah not in the 2.3 i have an upgraded hatch speed3 even with a timing chain its still far too weak to handle that much turbo even 8 seems far out. 10? No way it wont hold and thats too big a risk on those 2.3 Ford engines. Okay fine it holds 10 lbs and ratios are all solid for awhile but then transmission could act up too much forced induction is just way too stressful and you WILL blow up the motor. WWSKD? (What Would Scotty Kilmer Do) Not this i can assure you 100% and wouldnt advise anyone.

  • @JimmieZ89
    @JimmieZ89 4 года назад +3

    Damn this really sucks! I've been following your channel for a long time now watching and learning from your builds for when I finally do my MS3. How many miles were on your stock block at this time? You were making great power and it was nice seeing the runs back to back with the slight changes you made. Hopefully you get her back on the road soon with that built engine.

    • @WannabeTuners
      @WannabeTuners  4 года назад

      It had 154,000 kms (96,000 miles). Thanks man. We had about 10-15 minutes in between runs, but only 5 minutes between the 400 hp run, and the verification run when it blew. Can't wait to get built !

  • @mortysmith5556
    @mortysmith5556 4 года назад +9

    I know how much stress this is. But you should really document all your repairs and the build. I will be following along watching you!

  • @Muddysnowflake978
    @Muddysnowflake978 4 года назад

    I sorry to see you blew the motor now. It’s time to do some reach and build a beast of a motor. I hope nothing but the best for your future motor build

  • @ask4boost
    @ask4boost 4 года назад

    Worst feeling ever I'm sure.. but I cant wait see the process of building it 🤙🏽

  • @FocusedHands
    @FocusedHands 3 года назад +1

    Dang that was crazy!!! Good HP though!

  • @sq33qs
    @sq33qs 4 года назад

    All the best with fixing the car, GL.

  • @luistroll22
    @luistroll22 4 года назад +3

    Sorry for that, but its a new start, I'm stay here for see the progress guys

  • @RedClutch22_
    @RedClutch22_ 4 года назад +1

    Dude it’s all good ! You took it pretty cool I was sooo piss when I blew mines ! Now watch this mazdaspeed Reach to the next level

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      I'm just lucky I have another car to drive

    • @RedClutch22_
      @RedClutch22_ 4 года назад +1

      Lol my parents wanted to kill me ... I had no car for 6 months! ...

    • @WannabeTuners
      @WannabeTuners  4 года назад +2

      @@RedClutch22_ Oh man, it's crazy how we don't realize what we have until it's gone

    • @RedClutch22_
      @RedClutch22_ 4 года назад

      Dude Facts bro

    • @RedClutch22_
      @RedClutch22_ 4 года назад +1

      You can tell when the car was going into Boost the motor just took a Shit ... no fucks given ... you would think at high RPM it will blow at that moment but “GOING into boost” damn

  • @anthonycamillos3719
    @anthonycamillos3719 4 года назад +1

    Just thought I'd point out there probably wasn't much wrong except the stock internals only hold around 370hp at the wheels "safely". Looking forward to following your build!

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      Yeah and even with a conservative torque curve, anything can happen

  • @pitbulltrainingandmotorcyc1658
    @pitbulltrainingandmotorcyc1658 4 года назад

    How long did she last after the timing chain was done I’ve been fallowing your Chanel I’ve got an 06 ms6 I just did timing chain motor mounts cork sport fuel line wheel bearing bov optima battery I take and access port I’m aiming for reliability over power tho god I hope that she lasts i hope u build a new motor would love details on where to get one just Incase

  • @bananahammock789
    @bananahammock789 4 года назад +1

    This made me cry.

  • @nerygarcia978
    @nerygarcia978 4 года назад

    Is the cx7 engine the exact same engine in our cars ? Btw Sorry to here what happen bro , your speed 3 was one of my favorite out there . I know you’ll come back stronger and faster lol!!!

  • @blandry5014
    @blandry5014 4 года назад

    Any update buddy? I feel bad for you. Don't know what i would do if that happen to my speed3. hope to see that speed3 up and running soon. i like all your videos, keep on the good job !

    • @WannabeTuners
      @WannabeTuners  4 года назад

      Thanks a lot man! Right now the spare engine has been torn down and is awaiting it's built destiny at the machine shop. Tbh I'm glad it happened here rather than on the street.

    • @blandry5014
      @blandry5014 4 года назад +1

      it never fun when it happen but like you said better on the dyno then in the middle of downtown traffic or on the highway. Glad to hear that the engine is at the shop will be waiting for more videos.

  • @BL1THE
    @BL1THE 4 года назад +1

    :( rest in peace little axela

  • @Sugybanks
    @Sugybanks 6 месяцев назад +1

    What happened? I’m curious if the ring gap is just to small from factory on these for this kind of added power/boost

    • @WannabeTuners
      @WannabeTuners  5 месяцев назад

      We have a disassembly video of the carnage. Basically cylinder 2 connecting rod failed :(

  • @jeffreygonzalez8544
    @jeffreygonzalez8544 4 года назад

    I watched your video yesterday and I was like dam that sucks. Now on my way to work today I got rod knock bad. I’m in the same boat you are now

  • @Nevsack63
    @Nevsack63 4 года назад +2

    I really really like your MPS. Keep us posted on the aftermath and perhaps what failed ? Thx

  • @newground1341
    @newground1341 4 года назад

    Jeeze man, it’s “never enough”

  • @Anthony-vr3um
    @Anthony-vr3um 4 года назад

    Damn all good hope you find a good deal on a block and do some diy on porting the heads and 80lb springs. If you build it yourself it's very cheap I have a thread on mso but i did before mine blew so price may vary a bit block+machine shop

  • @BenjaminCorrigan
    @BenjaminCorrigan 4 года назад

    I feel your pain man. Mine blew 3 years ago.... :(

  • @angelavila2128
    @angelavila2128 3 года назад

    How many kms were on your car when you installed the bnr s4? Do you think your engine would have lived longer if you stayed around 350-370 hp range along with torque? I’m about to install a bnr s4 on mine as well but I’m a paranoid fuck.

    • @WannabeTuners
      @WannabeTuners  3 года назад

      The car had about 120,000 kms on it when we installed the BNR S4. I had been tuning the car since then using virtual dyno to estimate power. I found that virtual dyno read lower than the actual dyno that we went to, so if we go off of actual dyno numbers in comparison to VD numbers, up until it blew up on the dyno at 160,000 kms, the car was probably making anywhere from 350-400 whp depending on what tune I was running and how cold it was outside. Some theories I have that caused the engine to blow are that we were doing too many back to back pulls, the wot box acting as an ignition cut rev limiter (rather than the ECU's fuel injector cut) may have stressed the rods, or it was just it's time to blow. It's hard to say when these stock engines will let go, but the best thing to do is run an alcohol mix to prevent detonation, and run a safe consistent tune (not to say I wasn't lol)

  • @2011chitsazzadeha
    @2011chitsazzadeha 4 года назад +1

    Don't worry going built motor is great.

  • @kamaleon20002000
    @kamaleon20002000 4 года назад +6

    Is not all about fuel air ratio... playing with timing to get more hp is always dangerous.
    Life is full of lessons... repair and go for those 400 whp.

    • @2011chitsazzadeha
      @2011chitsazzadeha 4 года назад

      This definitely wasn't a result of the minor timing increases they did, the rods were probably stressed and gonna let go anyways. 12.5deg at redline is basically 93 octane levels of timing, nevermind the in-tank methanol.

  • @greentoolsnyc3985
    @greentoolsnyc3985 4 года назад

    Awesome stuff new sub for that

    • @WannabeTuners
      @WannabeTuners  4 года назад

      Lol all it took was for me to blow my engine

    • @greentoolsnyc3985
      @greentoolsnyc3985 4 года назад

      Sorry mate it happens at least u werent driving far from home like i was make more vids i will watch them

    • @WannabeTuners
      @WannabeTuners  4 года назад

      @@greentoolsnyc3985 Thanks dude, It could have been a lot worse. It worked out because I'm going built now so, should be fun!

  • @swiggityswagger1232
    @swiggityswagger1232 3 года назад +6

    400 whp is pushing the stock internals to its absolute limits dayum! I'm surprised it didn't happen before this dyno

    • @WannabeTuners
      @WannabeTuners  3 года назад +1

      Oh yeah it definitely had a good long run lol

    • @MrToastyman900
      @MrToastyman900 2 года назад +1

      400whp is surprisingly safe to run if you tune it right, i know people that daily 400whp stock motor cars, even one who’s managed to make 500whp on an unopened engine last quite a while

  • @wyattchilton15
    @wyattchilton15 4 года назад +1

    I'm a simple man, I see a speed 3 I hit subscribe. But I see neetronics I then hit the like button

  • @PH-x
    @PH-x 3 года назад

    Howmuch was it at the crank I only as cause a buddy of mine just brought one completely stock an broke his cv doing launches his butt dyno he told me was about 400nat the wheel but tis completely stock one cat has been removed an that's with a busted cv so I'm fallen it be from my buddy that is , be interesting to find out as his gauge only once read 18 but digital outputs from the obd2 onto my phone was only like 12-14ish psi would drop off above 6500rpm so it's fair to say tis was only about 250ish right? I recorded all of it on my phone an it had funky timing advancing never below 6.5 positive advance on the timing but it would spike up an down rapidly lol an he said he only uses half throttle but I was with him that sh3t was foot flat befor quarter throttle lmfao this just proves it man

    • @WannabeTuners
      @WannabeTuners  3 года назад

      If he's completely stock he won't be making more than 240 whp, but then again, numbers can vary. The only way to really know what his car is putting down at the wheels is to take the car to a dyno, and even then, all dyno's read differently

  • @I_Am_SoSo
    @I_Am_SoSo 4 года назад

    love them gen1. i have one also but i keep on getting misfire, rough idle and constantly dealing with crankshaft sensor. i replaced it but a week later it gives me the code again. any advice brother?

    • @WannabeTuners
      @WannabeTuners  4 года назад

      Try swapping coil packs to see if the misfire transfers to another cylinder. Also check crank sensor connections and related wiring for damage or shorts.

    • @I_Am_SoSo
      @I_Am_SoSo 4 года назад

      @@WannabeTuners the dealer swapped the motor with another replacemt and the fixed all the problems but i keep getting the same symptoms. i changed the coil packs so im thinking its the wires. i replace the maf sensor already also and spark plugs. 113k miles 😭

  • @coltonobriant6307
    @coltonobriant6307 4 года назад +1

    Is there a while thing of not flooring it under 3k? Maybe tomucg torque, idk just a guess from what i heard at a local meet i went too

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      When tuning you want to start a pull anywhere from 2500-3000 rpm to dial in as much of the usable powerband as possible. In the early days it wasn't recommended to floor it below 3000 rpm in 6th gear due to more load on the engine for a longer period of time. Nowadays the do's and dont's have been figured out, and the ability to tune the ecu to limit torque output below 3000 rpm has greatly helped to reduce engine failures. That being said, running a safe tune, with quality fuel is the most important thing. Personally whenever I am in 6th gear, I never floor it below 3k rpm ;)

    • @alexshoneya
      @alexshoneya 3 года назад

      @@WannabeTuners I dont wot below 3k at any gears...

  • @colinslager
    @colinslager 2 года назад +1

    How much power did it make at the crank?

    • @WannabeTuners
      @WannabeTuners  2 года назад +1

      If we look at what it made at the wheels, we can add about 10-15%

  • @adamswartz7670
    @adamswartz7670 4 года назад

    So sorry man. That sucks, kinda sounded like you windowed your block by sending a rod.

  • @Mazdaspeedgarage
    @Mazdaspeedgarage 4 года назад

    I’ve had bolt installed on the past on my speed3 and it was fun but now I have my speed6 I’m going the different route spend the money on a built long block that supports the hp I need

    • @WannabeTuners
      @WannabeTuners  4 года назад

      Yea and pack a fire extinguisher just in case

  • @mituc
    @mituc 4 года назад +1

    Oh no...:( Well, too many consecutive runs. I'm pretty sure that what happened is the classic phenomenon of piston rings butting and piston jamming against the cylinder wall. Happened to one of my friends I was tuning for. In his case it was #1 but it's really a matter of which cylinder has the smallest ring end gap for the heat already in the piston/cylinder.
    The good news is that with a built engine and the same mods you have now ( +WMI, never leave WMI out of the game) you can shoot for 600 (even though on a street used MS3 the practically usable limit is about 500bhp and 500-520lb*ft).
    P.S.: if you were spraying (WMI) this wouldn't have happened.

  • @dylanthomas9777
    @dylanthomas9777 4 года назад

    Why was the timing increased when you weren't making any large gains until it blew at 12.5?

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      According to the dyno graphs, from 9.5 to 12.5 degrees at 6700 rpm, it was generating about 10 whp more per degree at the same boost pressure!

  • @acu98mev
    @acu98mev 4 года назад

    hey i just picked up a speed3 im from hamilton area what kinda km did yours have when she poped

    • @WannabeTuners
      @WannabeTuners  4 года назад

      It had just under 160,000 km's

    • @acu98mev
      @acu98mev 4 года назад

      @@WannabeTuners dang mines got 376xxx

  • @ivanborruel
    @ivanborruel 3 года назад

    The cx7 turbo engine and the heads are the same as the mazdaspeed 3 1st Gen?

    • @WannabeTuners
      @WannabeTuners  3 года назад

      Yep the cx7 engines are the same in the gen 1's

    • @ivanborruel
      @ivanborruel 3 года назад

      @@WannabeTuners so that mean if my car is moddded, and I blew my engine off, I just bought a used cx7 turbo engine and swap it and thats it?

    • @WannabeTuners
      @WannabeTuners  3 года назад

      @@ivanborruel Well the turbo in the cx7 is slightly smaller, so you'd want to swap over the turbo from the speed 3. You'll also need to swap over the flywheel and clutch onto the cx7 engine by removing the flex plate and install a pilot bearing into the crankshaft.

  • @TBPony
    @TBPony 4 года назад

    Get one of those corksport built crate engines, they already have everything done for you for 500 plus, I have the same car with the same color so this was hard to watch

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      Thanks man, although I'm picking up a used running cx7 long block tomorrow which will be getting the treatment ;)

  • @bgbg7109
    @bgbg7109 4 года назад +1

    Its probally nothing you did.. with big turbo its not if but when!!!! Just curious why meth in tank when you ran aux fuel. Why not just e-85 mix??

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      Because we don't have E85 in the area

    • @TopiasSalakka
      @TopiasSalakka 4 года назад

      Lul E85 is a pump gas where i live

  • @amberheardslawyerprofessor5266
    @amberheardslawyerprofessor5266 4 года назад

    Ugh so sad. Hurts i have the 04 speed3 1st gen upgraded and would still have my heart sink seeing that. Yeah way too much stress on the engine. Stock engine cant handle that much piston and connecting rod or even just getting a small nut dislodging inside the engine. Definitely will need love and care. - ASE Firestone mechanic.

    • @WannabeTuners
      @WannabeTuners  4 года назад

      Don't u mean 2007 and up? Yeah man it was bound to happen sooner or later. Packing a fire extinguisher in the car from now on!

  • @muhsped3841
    @muhsped3841 4 года назад

    Can yall film the engine building process.

  • @br0leg274
    @br0leg274 4 года назад

    Hey, stock engine in Germany dies ~350hp at 20.xxx, direct or over time. Due to the high speed interstates we can see where the durability is.

  • @ibsilentops2897
    @ibsilentops2897 3 года назад

    are you ever going to get this back together?

    • @WannabeTuners
      @WannabeTuners  3 года назад

      Yes sir it's back up an running now, just need to finish editing the build video :)

  • @breakfasteatre
    @breakfasteatre 4 года назад +1

    It felt those tires on the car and commited suicide. Good luck with the build and send me a DM if you want a hand pulling the motor or putting it back in. I've done it multiple times

  • @ecsniping6850
    @ecsniping6850 4 года назад +4

    Every speed owners nightmare

  • @cliffscholes5966
    @cliffscholes5966 4 года назад

    This was a hard watch, knowing it was going to blow. I do think though that meth mix in the fuel tank is a very bad idea. And very unpredictable. And I think this is why you ha e a massive knock event, and blow a rod out the side. Fit a meth kit buddy. Much safer. I run 436bhp on stock block with a devilsown progressive meth kit. So my boost air temps are kept in check. I run 99ron (or octain as you lot call it) with meth kicking in at 15psi, and has full spray at 20psi. Hope this helps for the future build buddy.

  • @joshsmith4998
    @joshsmith4998 4 года назад

    Hey, the way I see it: Better this happens on the dyno than when you're out driving. That could be super dangerous if it happens during a street pull

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      For sure man! Packing a fire extinguisher from now on;)

  • @spillybuilt7491
    @spillybuilt7491 4 года назад +1

    What rpm was the tuner doing pulls from??

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      2500 rpm to 6700 rpm where the WOT box limits the revs through ignition cut, as opposed to the OEM fuel injector cut rev limiter

    • @spillybuilt7491
      @spillybuilt7491 4 года назад

      Stock blocks should really not do pulls under 3k

    • @CarlosGonzalez-vi9qv
      @CarlosGonzalez-vi9qv 4 года назад

      @@spillybuilt7491 All the tuners ask to go WOT after 2500 for the datalogs in 4th gear soo....

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      @@spillybuilt7491 That's what is recommend, but for tuning purposes most if not all tuners will start a dyno pull around 2500 rpm in order to tune that area of the rpm range

    • @spillybuilt7491
      @spillybuilt7491 4 года назад

      It was bound to happen at those power levels regardless. Best of luck on the rebuild!

  • @MatrixRC
    @MatrixRC 4 года назад +1

    No one noticed earlier the black smoke from the exhuast. Clear signs something is wrong. Just my mechanical experience. But you live and learn. You start modding and eventually this is the end result.

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      The black smoke is from the rich air fuel mixture and the blueish white smoke is from the turbo seal

    • @MatrixRC
      @MatrixRC 4 года назад

      @@WannabeTuners signs of tragedy about to happen.

  • @bryanmunoz4005
    @bryanmunoz4005 4 года назад

    Where are you located?

  • @Mazdaspeedgarage
    @Mazdaspeedgarage 4 года назад +1

    Another option you could go is a drop in ready long block from corksport or speed performance. I would go for stage 2 which supports 700++hp
    Just slap all your parts and your good to go

    • @WannabeTuners
      @WannabeTuners  4 года назад

      That is an option too! I'm just not sure if getting it done locally would be less expensive or not

    • @Mazdaspeedgarage
      @Mazdaspeedgarage 4 года назад +1

      Wannabe Tuners it’s not cheap to build a motor but it’s not easy either that’s why you gotta go to the right ppl who have been doing it for long time and who knows these cars
      Because you don’t want to have a built motor that wasn’t done right I’ve seen it happen

    • @raquielcross5757
      @raquielcross5757 4 года назад +1

      That's right better spend a bit more now that you re in this situation and get a safe reliable build than risk your money on a cheaper option

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      @@Mazdaspeedgarage Thanks for the advice :)

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      @@raquielcross5757 I know a reputable engine builder in the area called Competition Automotive. They've been around for over 40 years. I'll probably get an estimate from them first and go from there ;)

  • @Mazdaspeedgarage
    @Mazdaspeedgarage 4 года назад +2

    Not the results you want to see when you’ve spend your money 💰 on quality parts to achieve that satisfaction but keep your head up it could have been worse just means you gotta build your motor take your time with it do it right
    And do it right the first time so that won’t happen again

  • @OGtrushalpatel
    @OGtrushalpatel 4 года назад

    Blow up is at 6:03

  • @pitbulltrainingandmotorcyc1658
    @pitbulltrainingandmotorcyc1658 4 года назад

    Well that fucking sucks I was wanting to turn up the boost myself but I’m thinking I’ll leave her at stage one for now

  • @chrismullin3986
    @chrismullin3986 3 года назад

    They always blow up, even starndard, what was mazda thinking?? They need stronger internals, then we are talking some serious power!

  • @newground1341
    @newground1341 4 года назад

    Soooo You found another rig; 2nd gen’?

    • @WannabeTuners
      @WannabeTuners  4 года назад

      Haha we built another engine with forged pistons and rods

    • @newground1341
      @newground1341 4 года назад

      Fuck! When did you...did you shoot the build?

  • @Theromanticrejeck
    @Theromanticrejeck 4 года назад

    I lucked out and found a cx7 that was wrecked in the back and motor was good @ $450 USD. I recommend looking at a few in your area

    • @WannabeTuners
      @WannabeTuners  4 года назад

      Awesome! Yeah man that's the plan

    • @Theromanticrejeck
      @Theromanticrejeck 4 года назад +1

      Everyone always forgets about the cx7’s lol

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      @@Theromanticrejeck I should hopefully have a used CX7 long block by next week

    • @ivanborruel
      @ivanborruel 3 года назад

      The cx7 engine and head are compatible with speed3?

  • @geenuz4fam
    @geenuz4fam 4 года назад

    That sucks. My accord blew up on a dyno too. The price to pay when u wanna go fast. I learned that its not a good idea to wanna make your daily a race car. Goodluck with whatever you decide to do.

    • @WannabeTuners
      @WannabeTuners  4 года назад

      Thanks man! I'm picking up a used running long block today and am going to upgrade rods, pistons, and bearings

    • @geenuz4fam
      @geenuz4fam 4 года назад

      @@WannabeTuners 💪👍👍

  • @LikquidDutch
    @LikquidDutch 4 года назад

    Mine has been making about 370 on e85 for about 6 years on the stock motor on a bnrs3 scary i run her hard to but I have always had this fear in the back of my mind .

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      That's great to hear, I too have been around the same power level for years, always tuning on the street with 2 gallons on in tank methanol. This was actually our first time at the dyno. I have a feeling that abusing the ignition cut rev limiter from the WOT box after almost every pull might have stretched the stock rod, causing it to sheer as soon as torque started increasing. When it let go at 4300 rpm, it was only generating 320 ft lbs of torque. This is all speculation though. It very well could have just been its time. Either way, I don't think we'll have any issues occasionally using the WOT box with the built engine :)

  • @gimmethecarkeys
    @gimmethecarkeys 4 года назад

    Sucks brother... mine just cracked a ringland. Didnt explode like yours... judging by yours you will have to find a decent long block and rebuild it. Prob hit the valvtrain when it went boom boom.

    • @WannabeTuners
      @WannabeTuners  4 года назад

      Yeah dude consider yourself lucky. Take it easy on it and build her asap. I've already sourced a used running CX7 engine ;)

    • @gimmethecarkeys
      @gimmethecarkeys 4 года назад

      @@WannabeTuners mine is off at overspeed motorsports having the bottom end built. CNC ported head and valve springs done. Cant wait to see the upcoming content on yours!

  • @tylerallen4469
    @tylerallen4469 4 года назад

    Next chapter bud

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      Yeah man gonna put a rotary in it...more reliable 😑 jokes!

    • @tylerallen4469
      @tylerallen4469 4 года назад

      @@WannabeTuners oh geez! I just had to throw a gen 2 transmission in mine. Picked one up with only 40k on it. Probably one of the only benefits to torque steer is an abundance of lowish mile parts from ppl unknowing of torque steer. Almost all the cars you find have mild front passenger damage but all the good parts are still intact

  • @mazdaspeedg2380
    @mazdaspeedg2380 4 года назад

    Damn that sucks reason why I’m always scare to be on the dyno I’m making a lot less tho at 367whp

    • @MannyFresh1x
      @MannyFresh1x 4 года назад

      You always get that "dont blow up" feeling on the dyno

  • @linchester8464
    @linchester8464 4 года назад

    I not very experienced with MazdaSpeed3 engines but the Mustang Ecoboost 2.3L block shares some designs with the MazdaSpeed3 block aka the Mazda L engine
    looking up similar Mazda Zoom Zoom Boom and the Ecoboom situation
    putting aggressive boost levels combine with advance ignition timings is a recipe for disaster
    www.ozmpsclub.com/forum/general-mps-mazdaspeed-discussion/12879-how-get-400whp-your-speed-3-practical-way.html
    www.mazdaspeedforums.org/forum/f106/bad-news-forzda-1-blew-up-bent-77027/
    www.mazdas247.com/forum/showthread.php?123805882-Bent-Rod
    mechanics.stackexchange.com/questions/35750/timing-chain-jumped-probably-bent-a-piston-is-my-engine-worth-fixing
    it looks like there was knocking on the final run when the engine was really hot and it happened during the up stroke cycle and the con-rod/s just bent and snap under the high boost and detonation
    the bent/broken rods basically hit the sides of the cylinder and blew that chunk of the block and the rest of the components
    but def a engine tear down will reveal the damages and the cause of the failure.
    This is my assumption at this point based on my past experiences with blown Evo 4G63

    • @smtyson1650
      @smtyson1650 4 года назад

      The engine did sounded funny on that last run,right before the motor blew

  • @raquielcross5757
    @raquielcross5757 4 года назад +2

    Oh What!?!?at only 350 torque??
    I think maybe the car did too many runs in a row and needed to cool off before other triles..I m so sorry for you man that's a bummer now another load of money to rebuild it, atleast after that u d know you can easily pass 500 ponnies

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      Yeah man a build block is all this thing needs. I'm just looking to make decent jam reliably

    • @cliffordhaines6495
      @cliffordhaines6495 4 года назад +1

      Yeah I was wondering how long did he wait after each pull on it.

    • @WannabeTuners
      @WannabeTuners  4 года назад +2

      @@cliffordhaines6495 About 10-15 minutes in between runs. But only about 5 minutes between the 400 whp run and the vented block run lol. Definitely should have let it cool longer in between, but it goes to show that the block was ready to pop

  • @keonigaillard7804
    @keonigaillard7804 4 года назад +1

    Damn, that sucks man... Part out?? 😜
    Nah, I'm just playing. Time for full build. Send it!

    • @WannabeTuners
      @WannabeTuners  4 года назад +2

      No way I'm parting this thing out. I love boost way to much!

  • @TheOriginalPancakeHou5e
    @TheOriginalPancakeHou5e 4 года назад

    Just watching this, that’s sucks. These engines are hit and miss when pushing the limits. Mine made 520whp before it let go on stock rods and pistons. Bows the time to build so you can go further safely

    • @TheOriginalPancakeHou5e
      @TheOriginalPancakeHou5e 4 года назад

      I noticed you guys were throwing more timing at it instead of boost. Is there a reason why? I know most tuners prefer to add boost vs timing as timing creates more heat which of course cyl 3 is always producing more than any other. That’s what let go on mine

    • @WannabeTuners
      @WannabeTuners  4 года назад

      @@TheOriginalPancakeHou5e Yeah man it should be good when she's built and ready for action. When I tune I always dial in my boost and fuel curve first, and increase timing last. It's pretty much a balancing act between timing and boost, and too much of either will put more stress on the engine in general. I didn't want to run too much boost as I didn't want to cause inefficiency in the engines ability to breathe. I feel it runs better at 22 psi instead of 24 psi with these upgraded manifolds. We hear of people pushing big power on stock blocks, but that does not come without risk. I'd consider someone making 520 whp on a stock bottom end for a while quite lucky lol

  • @BigBoy-ub3uc
    @BigBoy-ub3uc 4 года назад

    What caused it?

    • @WannabeTuners
      @WannabeTuners  4 года назад

      I'm not exactly sure what caused it, although I'm thinking that the WOT box's abrupt ignition cut rev limiter feature may have stretched or fractured the cylinder 2 connecting rod, causing to break as soon as mid range torque was generated. With the stock block and a bigger turbo, it's not if it will blow, but when :) It's better to build it while it's still in one piece so you don't have to pay for another engine.

  • @SpiffyDay
    @SpiffyDay 4 года назад

    I’m surprised after adding 3 degrees of timing the tuner still added another full degree... sorry it blew.

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      I was the tuner! It's all good man, there's always risk involved when making this much power with a stock block

    • @SpiffyDay
      @SpiffyDay 4 года назад

      Wannabe Tuners of course!! Always a risk. That’s name of the game! Excited to see it back up and running hopefully soon

    • @WannabeTuners
      @WannabeTuners  4 года назад

      @@SpiffyDay Absolutely! We picked up a used running cx7 long block not long ago. Let the fun begin!

    • @2011chitsazzadeha
      @2011chitsazzadeha 4 года назад

      The timing was really conservative, realistically most speeds can run another 5-6degrees of timing on an ethanol mixture before getting close to the knock threshold.

  • @Ratcher.
    @Ratcher. 4 года назад

    mine went out while coming home at night on the highway whole car was in flames and light the whole highway like it was day got stuck at 3k rpms like it was redlining i have no idea where rod 3 went

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      Oh man sorry to hear, did the whole car burn down?

    • @Ratcher.
      @Ratcher. 4 года назад

      @@WannabeTuners no I had 2 extinguishers in the car and had to use both but i saved it haven't looked over the whole wiring harness the bottom of the car is crispy though lol. Good luck with yours though I will say don't let the car sit to long with out progress like i did after 2 years you will lose motivation sooo fast you'd wish it did burn to the ground.

    • @WannabeTuners
      @WannabeTuners  4 года назад

      @@Ratcher. Haha alright man thanks for the advice;)

  • @urbandadtv
    @urbandadtv 4 года назад +2

    Damn after like the 4th time i was like shit that engine taking some abuse! Is that normally how a Dyno works?? i would think the shop has to have some responsibility here no? sorry this happened dude, i love the vids you guys did for the mk5.

    • @WannabeTuners
      @WannabeTuners  4 года назад

      Thanks brother! All the tuning was done by me, so the shop cannot be blamed

    • @thomascarpenter5536
      @thomascarpenter5536 4 года назад

      Dyno is the best way to tune and that is standard. Something else went wrong.

    • @MannyFresh1x
      @MannyFresh1x 4 года назад

      Also when you get tuned by a shop most times they make you sign a waiver. Meaning if they suck at tuning and blow your car up they arent held accountable. Its just to cover their ass.

  • @emmanuelguerrero6598
    @emmanuelguerrero6598 4 года назад

    Can anyone help me out with my boost problem?
    I was hitting about 16 psi then 13 after about9 and at times I dont even feel the boost what should I check ?

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      Email us a data log of when it happens. Also check for any boost leaks.

    • @emmanuelguerrero6598
      @emmanuelguerrero6598 4 года назад

      @@WannabeTuners I put a smoke machine on it and didn't really see anything. Is there certain spots of the car I should check ?

    • @WannabeTuners
      @WannabeTuners  4 года назад

      @@emmanuelguerrero6598 Not really. It could be a lot of things. What mods do u have on the car?

    • @sav7123
      @sav7123 День назад

      Either a boost leak or injector seals

  • @ProChargedLS2
    @ProChargedLS2 4 года назад +1

    Y i k e s. With how everything has gone with my car I predict mine will blow the next time I drive it every single day. Not a fun way to own a car. It's known across the forums 400whp is the absolute max for stock internals, why keep pushing, just sheer curiosity?

    • @WannabeTuners
      @WannabeTuners  4 года назад

      Well the first pull we did made 378 whp. That same map made 340 whp in virtual dyno on the street with CF 1.01, so since I've been tuning my car on the street, it's possible that it's been making more power than I thought. The reason I kept going with it was because I've ran more ignition timing in the past when tuning on the street, but never this much boost. Usually 22 psi with 11 degrees at 6k rpm. So either it's a coincidence that it blew on the dyno and not the street, or that little bit more boost was a little too much, or hitting the rev limiter with back to back runs stressed the components beyond what they could handle. Tbh I'm happy it happened on the dyno and not the street! This forces me to build, and the last thing I want to do is sell the car!

    • @ProChargedLS2
      @ProChargedLS2 4 года назад

      @@WannabeTuners Yeah fair enough! Was probably a lot of things building up to the boom. Sure are lucky it happened there. Just curious but how much oil seeped into the dyno lol

    • @WannabeTuners
      @WannabeTuners  4 года назад

      @@ProChargedLS2 Ohhh there was a lot of oil that seeped into it. There was oil all under neath the vehicle. Hopefully oil doesn't damage their dyno.

  • @matthewlucie
    @matthewlucie 4 года назад

    RIP

  • @MrDeriktaylor
    @MrDeriktaylor 4 года назад

    Mine build was over 10k like 7 years ago I'm sure it's more now. Good luck

    • @WannabeTuners
      @WannabeTuners  4 года назад

      10k usd? What all was done?

    • @fsflip3111
      @fsflip3111 4 года назад

      10k? investment? or miles on car?

    • @lonewanderer958
      @lonewanderer958 4 года назад +1

      I highly doubt you paid 10k To build a 3 motor 😂😂😂 what ya goin for 1000 hp? 😂😂

    • @MrDeriktaylor
      @MrDeriktaylor 4 года назад

      10 for motor, exhaust,turbo kit,etc

    • @MrDeriktaylor
      @MrDeriktaylor 4 года назад

      @@fsflip3111 invested

  • @geraldgoodiii6993
    @geraldgoodiii6993 Год назад

    Damn .. u guys run mad low timing compared to us in the KDM land
    19-21* is around what most run
    Some guys talk about 27-28* .. I’m like uhhh 😬

  • @geraldgoodiii6993
    @geraldgoodiii6993 Год назад

    Good god so hard to watch. When I went on dyno to see what power I made I was holding my breath each oull .. so many nightmsre stories about dynos and vids of blown up motors

    • @WannabeTuners
      @WannabeTuners  Год назад

      Yeah I definitely didn't expect my first dyno experience to involve my engine blowing haha

  • @ghost-4230
    @ghost-4230 4 года назад

    Holy Jesus

  • @journalsofajackass6195
    @journalsofajackass6195 4 года назад +1

    Sell me that guardian angel. Lol

    • @WannabeTuners
      @WannabeTuners  4 года назад

      I'm definitely gonna need it when we drop a built engine into this thing ;)

  • @geraldgoodiii6993
    @geraldgoodiii6993 Год назад +1

    Those jagged lines are showing possible misfires
    Shouldn’t look like that

    • @WannabeTuners
      @WannabeTuners  Год назад

      It's very possible, we did notice some abnormal knock values in some of the pulls

  • @sbscars
    @sbscars 4 года назад

    Hopefully I'm not next to ZZB. I'm just down the road from you guys, so I hope it's not contagious.

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      I really do wonder if the WOT box had something to do with it

    • @sbscars
      @sbscars 4 года назад +1

      @@WannabeTuners funny enough the guy I bought my sway bars off of ZZB at Neetronics as well. Only with a GTX3071 and a spike of 32ish psi. Made around 500 when it popped though (or so I was told), he was from Milton and also drove a white gen juan.

    • @WannabeTuners
      @WannabeTuners  4 года назад

      @@sbscars Oh damn what did he have done to the car? Stock block?

    • @sbscars
      @sbscars 4 года назад

      @@WannabeTuners Yep, stock block. Supporting mods from what I can remember were:
      -Sure Motorsports turbo header (Which I bought off him)
      -ATP Turbo GTX3071R externally gated to a 38mm or 44mm Tial (don't remember the exact size)
      -3" catless turbo back
      -TR8 FMIC w/ CX racing piping
      -CPE injector seals
      -Aux fueling w/ split second controller
      -3.5" intake
      -unsure what intake manifold he was using because it was already sold when i went to pick up the sway bars and turbo header.
      His name was Imran if i remember correctly, his ad was on the facebook market place back in March 2019 when I met up with him. Super nice guy.

  • @jessebudelman
    @jessebudelman 4 года назад

    What what caused failure do you think?

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      I'm not exactly sure. I've never had issues one the street with a similar tune. The difference is that on the street I always shift before the WOT box's ignition cut type rev limiter. I wonder if the random cutting of the ignition system under high engine load at high rpm stresses the engine components enough to weaken them.

    • @jessebudelman
      @jessebudelman 4 года назад

      Damn, that’s shitty....watching all that hard work just to Grenade the engine makes me sad. Wishing for a speedy recovery of the Mazda.

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      @@jessebudelman Thanks man, she'll be back up and running with a built engine soon :)

    • @jessebudelman
      @jessebudelman 4 года назад

      Bitchin’! Can’t wait to see it. Makes me wanna find a low milage 2.0 ecoboost and build my own engine for my ST! Haha

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      @@jessebudelman Yeah man go for it!

  • @backroadboosters4017
    @backroadboosters4017 4 года назад +1

    These motors don’t like to hold more than 350ft lbs of torque. That was highly likely the failure point; the rodssss

    • @WannabeTuners
      @WannabeTuners  4 года назад

      That's exactly what happened, the cylinder 2 rod sheared causing some serious damage. We have a teardown video showing the carnage

  • @gunssuh4722
    @gunssuh4722 4 года назад

    No way! Nice rims tho.

    • @WannabeTuners
      @WannabeTuners  4 года назад

      Yeah I love my cheap (inexpensive) wheels

  • @newground1341
    @newground1341 4 года назад

    💰

  • @btshader
    @btshader 4 года назад +2

    is it just me or does the engine have a funny sound on the last run?

    • @WannabeTuners
      @WannabeTuners  4 года назад

      In the data log it was pulling over 5 degrees of timing for several cells right before it blew. We're not sure if it was just noise from a stressed component, or if it actually was detonating (which doesn't seem feasible as it was running 94 octane with 3 gallons of in tank methanol)

    • @btshader
      @btshader 4 года назад

      @@WannabeTuners could be due to the noise from a stressed component, keen to see what it looks like when u open it, i built my motor like 4 months ago and have to say u will enjoy doing it, stay positive and good luck bud!

    • @WannabeTuners
      @WannabeTuners  4 года назад

      @@btshader Thanks man! I take it u got everything machined at a shop, and then assembled it yourself?

    • @byteoncomputerservices8054
      @byteoncomputerservices8054 4 года назад

      That sounded like LSPI. Not uncommon in DI engines unfortunately.

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      @@byteoncomputerservices8054 It blew at 4300 rpm generating only 320 ft lbs of torque based on the dyno graph. It was running 94 octane with 3 gallons of in tank methanol, so pre ignition and detonation should not have been an issue. But, anything is possible. That dip in power that u could hear was over 5 degrees of timing being pulled right before it let go. Wether it was knocking, pre igniting, or just noisy from a stressed component, taking it apart should be pretty interesting, and hopefully we can get a clearer idea of how it failed :)

  • @lambo5965
    @lambo5965 2 года назад

    That car sounded unhealthy from the very first pull. They just have that weird sound when they are about to go in high rpm I've learned.

  • @daltonpacheco2746
    @daltonpacheco2746 4 года назад

    Oh no! 😕

    • @WannabeTuners
      @WannabeTuners  4 года назад

      Yeah man maybe I had a weak stocker blocker

  • @zignimus5334
    @zignimus5334 3 года назад

    Lost my job with a 12 month old to support. Went bankrupt do had to buy a car. 6000$ on a mazdaspeed 6 and didnt even last 1 day..

  • @jimmytran5328
    @jimmytran5328 4 года назад

    Why would you run it that many times only 10-15 minutes in between and then 5 minutes between the 400hp.... like dam... what a waste...

    • @WannabeTuners
      @WannabeTuners  4 года назад

      It's part of the game, better it happened here than on the street!

  • @trey369
    @trey369 4 года назад

    Nooo monicaaa..

  • @groundhabit6408
    @groundhabit6408 4 года назад

    Torque is what killed your block ... You guys should have called it a day after hitting 350wtq numbers ... You can't push these stock blocks on higher torque or this will happen ... And if this dyno-jet wasn't calibrated correctly and read lower , you were playing with fire without even knowing it

  • @numinous4789
    @numinous4789 4 года назад

    Dang, that stinks. Seeing the title, I was puckering during the vid, haha. This is the ZZB story you always fear - on the dyno during WOT. Amazingly, most ZZBs occur in casual, daily driving, not even during WOT. It looks like it let go around the peak torque rpm range too, but your numbers were easily in what's considered "safe" for stock-block range.
    Mileage on the motor? How long at this power level? Something for sure wasn't right if you were getting 5.xx KR with the level of octane you had in light of the timing you were running. That KR points to maybe ringlands, bearings, or rods already having issues, perhaps, and this was just the last straw. Well, build it stronger and come back better than ever! XD

    • @WannabeTuners
      @WannabeTuners  4 года назад +1

      Thanks dude! It had about 158,000 km's on the clock. Based on the way I've been tuning it over the years and according to this dyno, it's been in the 340-380 whp range for about 40,000 km's since installing the BNR S4. Virtual Dyno read a little lower than this dyno. We read and hear a lot about how stock blocks can take quite a bit of abuse, and it's been proven time and time again that they can. But based on how fragile the stock rods and pistons look, I'm not surprised. We found time to take the blown engine apart just yesterday and will be uploading a teardown video very soon. The damage is pretty bad and it's hard to say what caused the failure, but hopefully someone can give us a better idea :) The machine shop should be starting work on our used CX7 long block in the next week or two, so it's just a matter of being patient and excited at the same time lol