My Quadcopter with APM 2.8 not giving stable flight and fliping

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  • Опубликовано: 3 окт 2024

Комментарии • 24

  • @anuragmd6980
    @anuragmd6980 3 года назад +4

    Check motor rotation, or esc connection

  • @uandeleon290
    @uandeleon290 3 года назад +3

    Perfectly Cuts Screams/Flip

  • @maulanawahyudi7127
    @maulanawahyudi7127 3 года назад +1

    Biasanya cw / ccwnya dari baling baling, kalo udah bener urutan motornya ke fc kalo di pixhawk

  • @praveshsingh9973
    @praveshsingh9973 3 года назад +3

    In APM you have to input the esc signal cables in this way -> 1342 where 1 is right front motor,3 is left back motor, 4 is left front motor and 2 is right back motor. I am 100% sure that this will work.
    And you are not having any calibration issue as i can see. Everything’s fine. Just do what I said.

  • @anasmirkar7494
    @anasmirkar7494 3 месяца назад

    Arrange cw propeller and ccw propeller in proper order to generate thrust downside.

  • @davitannous302
    @davitannous302 3 месяца назад

    Did you fixed it? How?

  • @ardiansyah-nr3km
    @ardiansyah-nr3km 4 года назад +1

    Malah ambruk karo ambyar Yi... 😂😅😅😅

    • @MindoLab
      @MindoLab  4 года назад

      Itu contoh yg blm fix mbah ardiyansyah hahaha

  • @kentdaimlerlibo-on1832
    @kentdaimlerlibo-on1832 5 месяцев назад

    Hi, have you managed to solve it? If yes then how?

  • @lolstudy4062
    @lolstudy4062 4 месяца назад

    Motors connection is not correct and on the right side

  • @PirinikoS85
    @PirinikoS85 3 года назад +1

    check propeler rotetion wrong

  • @TrueExperiment02
    @TrueExperiment02 2 года назад

    Trim the transmiter

  • @haidarbutuh493
    @haidarbutuh493 4 года назад +1

    Hihiii

  • @viveksingh-oh3gs
    @viveksingh-oh3gs 3 года назад +1

    baccho ka kaam ni udhana 🤣

  • @SanthoshMuruganantham
    @SanthoshMuruganantham 3 года назад +2

    Calibration problem

    • @MindoLab
      @MindoLab  3 года назад +1

      i have tried the calibration endlessly and finally i gave up

  • @creativeunboxing2288
    @creativeunboxing2288 3 года назад

    No all of you check to that child's when he thortlle up to 50% he pull the liver at right side

    • @MindoLab
      @MindoLab  3 года назад

      I think the calibration is not good, but I've tried repeating the calibration, the problem is still the same. the second issue is the flight control APM, it has been broken from the seller on aliexpress

    • @creativeunboxing2288
      @creativeunboxing2288 3 года назад

      Yes I think that was the problem you telling that it was broken then it have been problem in gyrometer. If the problem is not then check the balanceof drone if it straight at mid point then it will ok otherwise if till rightward or leftward then that side was heavy side

  • @yus8085
    @yus8085 3 года назад +1

    Salah masang baling baling kali gan? Saya pernah soalnya karna salah masang

    • @MindoLab
      @MindoLab  3 года назад

      sy punya drone satu lg pernah kasus sama bgt tp setelah dibalik baling2nya hasilnya bisa terbang. tapi kalau yg ini sampe pusing bolak baliknya tetep aja gan