NBR Works
NBR Works
  • Видео 17
  • Просмотров 1 387 147
Hung by a Single Point Thread!
Build video of an auto-retract threading tool for the lathe.
*Patreon:* www.patreon.com/nbrworks
*Tools I use:* www.nbrworks.com/tools/
*KBC Tools & Machinery*
Edge vice stop: www.kbctools.com/itemdetail/1-811-14000
Noga deburring tool set: www.kbctools.com/itemdetail/1-457-525
Cratex stick: www.kbctools.com/itemdetail/1-614-6404M
Inspiration videos:
Mr. Whoopee's threading tool: ruclips.net/video/IkVTmoTLeWs/видео.html
Cut knurling: ruclips.net/video/jNCAGeJN01A/видео.html
Просмотров: 125 210

Видео

Engraving Metal with EM Smart's Fiber Laser
Просмотров 2,7 тыс.2 месяца назад
For EM Smart laser purchases: the coupon code *NBRWorks* will give you an additional discount of 100 USD/EUR over the current EM Smart laser prices. EM-Smart US site: bit.ly/4ee1UGv EM-Smart EU site: bit.ly/3NeBCIP My Patreon: www.patreon.com/nbrworks Tools I use: www.nbrworks.com/tools/ Have you ever used a fiber laser at home? What do you use it for? I've had mine for about a month and the po...
Machining a bearing spacer: how hard can it be?
Просмотров 49 тыс.5 месяцев назад
I was asked 2 bearing spacers, so I made 7. Typical newbie... Tools I use: www.nbrworks.com/tools/ Chronos Ltd website: www.chronos.ltd.uk/ - Dasqua parallel set: www.chronos.ltd.uk/product/dasqua-precision-machinist-tools-premium-parallel-bars-set-with-aluminum-case/ - Dasqua digital indicator: www.chronos.ltd.uk/product/dasqua-absolute-digital-dial-indicator/ - Dykem engineers blue: www.chron...
Let's face it, no one does this on the lathe.
Просмотров 400 тыс.7 месяцев назад
A whole lot of work to get this right, but the result... I'm happy! Tools I use: www.nbrworks.com/tools/ Thanks Joe Pie for the idea: ruclips.net/video/J1RFTRzuAcU/видео.html #lathe #diy #machineshop ruclips.net/video/M5UhrqSyetk/видео.html
Driving ANYTHING between centers on the lathe.
Просмотров 124 тыс.9 месяцев назад
How do you drive stuff between centers? Here's my take on a driver for the metal lathe. Tools I use: www.nbrworks.com/tools/ And thanks to Joe Pie for sharing: ruclips.net/video/U3x8H1Xb-jg/видео.html #lathe #diy #machineshop ruclips.net/video/5qYqlkox28A/видео.html
Will a diode laser engrave STEEL? Aluminum? Brass?
Просмотров 9 тыс.10 месяцев назад
We all know a diode laser can engrave stainless. What about 4140? ... and brass? aluminum? Tools I use: www.nbrworks.com/tools/ Timestamps: 00:00 The one and only 4 stroke laser engraver 00:53 Creality Falcon2 01:56 Basics first 06:30 The Dovetail Cutters are back! 08:56 Cutting silicon rubber 10:00 Marking Metals (4140, aluminum, brass) 13:58 Final thoughts Creality Falcon2 22W: s.zbanx.com/r/...
I made a dovetail cutter... or two...
Просмотров 101 тыс.Год назад
I thrashed a dovetail cutter, so I made another one. But that's not all. Tools I use: www.nbrworks.com/tools/ Timestamps: 00:00 I did it again 00:40 Machining a new dovetail cutter 10:30 Re-sharpening an HSS dovetail cutter 12:42 U3 grinder dividing head - the challenge with 10 flute cutters 14:52 Testing the new cutter #lathe #diy #machineshop ruclips.net/video/-gWCOr1DtJU/видео.html
Parting-off on the Lathe - Rigidity, Rigidity... and a Spring!
Просмотров 266 тыс.Год назад
After upgrading my lathe to use a solid tool post mount, I'm looking to further improve its capability to part-off stock. Curiosity took the best of me this time and I'll be making a Spring type part-off tool holder to support 2 different blades. Tools I use: www.nbrworks.com/tools/ Blade used in the video (affiliate link): amzn.to/47jsJWx Timestamps: 00:00 Hello 00:19 My new part-off blade 01:...
How a Solid Tool Post Mount changed my lathe
Просмотров 153 тыс.Год назад
Parting or cutting off steel has always been a challenge on my lathe. Issues range from heavy chatter to broken inserts and tools which end up stalling the motor and sometimes damaging the work done on a part. Today we're making a solid tool post mount to replace the compound (top slide). The compound on small lathes is known to have rigidity issues and that's what we're looking to upgrade. Too...
A spindle walks into a test bar... WHAT?!
Просмотров 11 тыс.Год назад
When I was rebuilding my lathe I got a test bar to help me check the headstock alignment... but instead, it took me down an endless road of tests and uncertainty. While counting tenths is still my favorite sport, I decided to take a break and put this video together so you can join and count with me. Tools I use: www.nbrworks.com/tools/ Lathe: HBM 250x550 Profi Vario Lathe rebuild playlist: ruc...
Lathe rebuild Pt.3 - Final episode
Просмотров 12 тыс.Год назад
Welcome to the last episode of my HBM lathe rebuild series. Today we're going to replace the 3-jaw chuck with a 6-jaw, rebuild the tailstock and have a look into a problem I run into in the early stages of the rebuild. After that we'll go through the necessary adjustments to align the lathe so that a straight part can be cut. This includes the tailstock alignment. The video ends with a quick wo...
Lathe rebuild Pt.2 - The apron, a quick change tool post and something about the gearbox
Просмотров 19 тыс.Год назад
Hi everyone. This is the second part of my HBM lathe rebuild. We'll go through the apron where I spent hours deburring all the parts (but that's boring, I'm saving you from that), then we'll replace the 4 way tool post with an Aloris replica (wedged quick change type) and finally we'll look into the gearbox that allows to reverse the direction of the lead screw and easily select one of 3 feedin...
Lathe rebuild Pt.1 - The bed, the saddle and the headstock
Просмотров 14 тыс.Год назад
Hi everyone. In this video we'll go through part of the process of my lathe rebuild. There might be a few things missing (like 'levelling' the bed before anything else), it was too much footage to squeeze in a short video. Anyway, I hope this helps someone out there; at least you can look at some parts of the lathe that you couldn't otherwise without taking it apart. Tools I use: www.nbrworks.c...
Calibrating an inside micrometer
Просмотров 3,3 тыс.Год назад
I had this old Bowers internal micrometer offered in a non-working condition. In this video I will take it appart and find out how to calibrate it. I hope this might help someone with a similar micrometer. Tools I use: www.nbrworks.com/tools/ 00:00 Introduction 00:27 Tool description 01:09 Condition check - out of calibration 02:43 Disassembly and inspection 06:46 Fixing spindle backlash 08:02 ...
Machining an ER32 collet chuck
Просмотров 84 тыс.Год назад
Today we are machining an ER32 collet. This tool will help press fitting thin long rods in a shop press. The collet chuck will be fitted to the end of the piston and there's a jig on the press plate to keep things repeatedly in place (and square). The chuck has no through hole as the the bottom of the ER taper will be pushing the rods down, not the collet. Tools I use: www.nbrworks.com/tools/ 0...
Making new shafts for SU H2 carburettors and skimming original butterflies
Просмотров 6 тыс.Год назад
Making new shafts for SU H2 carburettors and skimming original butterflies
New HBM 250 x 550 metal lathe: Unboxing and Dismantling
Просмотров 11 тыс.2 года назад
New HBM 250 x 550 metal lathe: Unboxing and Dismantling

Комментарии

  • @fredfowler4364
    @fredfowler4364 День назад

    Hi, Fred Fowler here. Nice videos! I was the owner of Fowler Tools and I am happy to see you using some of our instruments like the NSK Mechanical digit mics and Bowers bore gages in your work. Quality work!

    • @nbrworks
      @nbrworks Час назад

      Hi Fred. That's very cool, I wonder how this video was suggested to you. The Fowler/NSK micrometers are my go to mics. I have 3 of them, 0-75mm, all bought in second hand and clean/rebuilt by me. They're accurate, reliable and I trust them. I also like how they feel in the hand, they're well balanced. The mechanical digits are nice to show measurements for the camera. As for the Bowers internal micrometer, it was given to me by a family member, who didn't understand how it worked (out of calibration). I just wished it was smaller, I would use it a lot more! Thanks for stopping by and the comment - amazing what the internet can do 🙂

    • @fredfowler4364
      @fredfowler4364 58 минут назад

      @@nbrworks Thanks for responding! As I am a machinist at heart, I follow a number of channels on YT like Old Tony, Abom, Clough, CEE, etc... - Yours happily popped up on my feed one day and I took an immediate interest! Back in the 80's, I interned at a number of precision instrument manufacturer's like Trimos, Sylvac and Wyler in Switzerland and Bowers, British Indicator (Verdict) in the UK. It was part of learning the business from the ground up. No better way to learn the tools than to make them! Now that I'm retired and sold the tool business, I run a small woodworking & CNC shop doing odd jobs to keep busy and I have access to a metalworking shop as well. I also stay involved with Fowler in a limited way and keep up on the industry trends. Pleasure to meet you and I look forward to future content, keep up the great work! F

  • @takedeadaim8671
    @takedeadaim8671 День назад

    I do threads up to shoulders all the time and have found the easiest way is to use a left hand tool upside down and run in reverse. I set a carriage stop that I can return to on each pass. The depth of thread is easy to calculate and thus so is the depth. Of the clearance groove. The width of the groove is consistent based on the threading tool used. Since I’m not threading toward a shoulder or the chuck, the stress of the job is gone.

  • @JFirn86Q
    @JFirn86Q 2 дня назад

    That wrinkle finish is so good!

  • @Hichamhasan
    @Hichamhasan 2 дня назад

    You've machined a little human ! 🙃 👶

    • @nbrworks
      @nbrworks 22 часа назад

      They're getting expensive so I made my own 🙃

    • @Hichamhasan
      @Hichamhasan 7 часов назад

      @@nbrworks pragmatic 🧠

  • @Michal_Sobierajski
    @Michal_Sobierajski 4 дня назад

    That's a lot too much rpm on reamer 🤦🏻‍♂️

  • @pgsibilo
    @pgsibilo 4 дня назад

    AWESOME 💯💯💯

  • @ohar7237
    @ohar7237 5 дней назад

    Hey, at least you're making custom fixtures for something you plan to do more than once...

  • @AndrewCampbell-ut6jk
    @AndrewCampbell-ut6jk 6 дней назад

    The shaft hole needs to be bored, the reamer will follow the hole and drilling is not good enough.

  • @JulianMakes
    @JulianMakes 7 дней назад

    Absolutely brilliant project, also all the little extra bits were superb. Really brilliant. Thank you

    • @nbrworks
      @nbrworks 22 часа назад

      Thanks Julian!

  • @charlieromeo7663
    @charlieromeo7663 8 дней назад

    Nice work.

  • @eboneezeradams1821
    @eboneezeradams1821 8 дней назад

    Nice effort but kinda a long way the wrong way. Use a geometric die head instead. Fast,and will get you closer to the shoulder.

  • @HiVoltish
    @HiVoltish 9 дней назад

    Bravo!!

  • @tiborbienenstein6484
    @tiborbienenstein6484 9 дней назад

    Fortunately in my shop we have a lathe wich stops going forward automatically as soon as it hits the carriage stop. Sorry for bad spelling I am Austrian and don’t know all those specific words in English 😂

  • @kevinsellsit5584
    @kevinsellsit5584 10 дней назад

    Three things stand out about 4:36 #1 a loud noise. #2 change of insert was required. #3 Change of underwear highly recommended.

  • @jacobosgood3513
    @jacobosgood3513 11 дней назад

    So many times when I watch RUclips machining I cringe when forced to watch the makers power tapping with conventional taps, seeing you hand tapping with power taps was a nice balm on my soul.

  • @raysimon1368
    @raysimon1368 13 дней назад

    This is something I have been going to make for my sheldon lathe for years you done a nice job and the results show it anyone can run a big lathe and take big cuts because they are so ridged with all the mass of cast iron but a 6mm cut on a mini lathe even though it was 12L14 is impressive my lath will not do it and it is larger than his taking the compound off and on when you need it isn't bad on a small lathe just a hassle but i do know from past experiences thatit is worth it from a retired machinist thanks for sharing

  • @leanderdrefahl1430
    @leanderdrefahl1430 14 дней назад

    Thumbs up and comment after 3 minutes...man i love content like this❤😅 greetings from Germany

  • @RonBateman-vl2wz
    @RonBateman-vl2wz 14 дней назад

    Might I ask what size lathe this is?

    • @nbrworks
      @nbrworks 14 дней назад

      Hi. It's 250x550, check out my other videos. Thanks

    • @RonBateman-vl2wz
      @RonBateman-vl2wz 14 дней назад

      @@nbrworks Hey thanks for the quick reply and I will.

  • @garymucher4082
    @garymucher4082 19 дней назад

    Was wondering if it could work on PC board material. If it could etch/engrave copper clad, it would work great for making circuit boards. IDK but will find out with our new one we received...

  • @JRC45
    @JRC45 21 день назад

    Love you grinding machine. Where did you get it? Who makes it? It notes nice.

    • @nbrworks
      @nbrworks 22 часа назад

      Hi, it's from HBM, from the same place where I got the lathe. Look up for U3 universal grinder, that's the one. I believe the latest model is the U5, I don't know which upgrades it has, if any.

  • @Probsnawt
    @Probsnawt 21 день назад

    Did you try taking the bore to size after the threading operation?

  • @peterhalstead7281
    @peterhalstead7281 21 день назад

    Very nice but over complicated.👍

  • @grahamhall2662
    @grahamhall2662 22 дня назад

    Wow that was a fantastic demonstration and I learned a lot. With regard to the broken tap, perhaps you could have backed it off on a regular basis to break the chip, swarf, that is the way I was taught but you know a lot more about this than myself? Great save however. Subbed.

  • @thearkone
    @thearkone 22 дня назад

    why reinvent the wheel?? just use an acorn die in the tail stock

  • @db45acp89
    @db45acp89 23 дня назад

    Excellent process and work. Kudos on the removal of the broken tap! Any chance you have a drawing/ dimensions for this? I didn't see one mentioned. Thanks for the great video. Subscribed based on this.

  • @richardphillips8652
    @richardphillips8652 24 дня назад

    Amazing work. good skills.

  • @fertiv5_67
    @fertiv5_67 24 дня назад

    полная ерунда. Жесткости ноль. Резьба рваная, резец дробит. Хуня

  • @adfy2307
    @adfy2307 24 дня назад

    CNC? -❌ Overenginired stuff - ✅

  • @greglaroche1753
    @greglaroche1753 24 дня назад

    Great job! Thanks for the video.

  • @jeffbertsch5917
    @jeffbertsch5917 24 дня назад

    My butt quivered watching you cut that piece on the bandsaw.

  • @MrRctintin
    @MrRctintin 25 дней назад

    Wow, I love that tool!

  • @merlinmagnus873
    @merlinmagnus873 25 дней назад

    Cool design. Never seen that before. Using a bi-stable pair of springs instead of an over-center design would get the same result for keeping the mechanism locked.

  • @paulconrod4504
    @paulconrod4504 25 дней назад

    well done mate

  • @yollayolla3929
    @yollayolla3929 25 дней назад

    Nice

  • @richhuntsd12
    @richhuntsd12 25 дней назад

    Really great video and keep up the cleaning. Awesome little tool!!!

  • @theperl9663
    @theperl9663 25 дней назад

    Nicely done

  • @ftlw1433
    @ftlw1433 25 дней назад

    You are very skilled. I wish machining was a cheaper hobby.

  • @johnmignano7872
    @johnmignano7872 26 дней назад

    👍👍👍 good tips and tricks

  • @homemadetools
    @homemadetools 27 дней назад

    Great work. We shared this video on our homemade tool forum last week 😎

  • @bryanwanek46
    @bryanwanek46 27 дней назад

    That's an awesome parting tool holdet! Well done sir. I may have to attempt making one.

    • @nbrworks
      @nbrworks 26 дней назад

      Cool. Let me know how it goes. Nowadays I mostly use carbide to part off steel, but was this tool holder that taught me how much pressure and speed I should use. It helped developing that feel and confidence needed for the parting operation.

    • @bryanwanek46
      @bryanwanek46 24 дня назад

      @nbrworks I hate parting. A little too much feed and chink, there goes your carbide insert. Not enough and you are just rubbing the workpiece and not cutting. I wish there were unicorn settings for speeds and feeds that would always work. I love how your setup incorporates the spring up in the nose of the holder. Just elegant. Great work!

  • @patrickmazzone9066
    @patrickmazzone9066 27 дней назад

    Awesome tool good luck

  • @bullshitvendor
    @bullshitvendor 29 дней назад

    ugh! how much is a lathe in this size that _doesnt_ require a rebuild straight out of the box 😵‍💫

  • @yveslegrand9826
    @yveslegrand9826 29 дней назад

    I took part of your idea to work on my 1979 Suzuki TS 125ER carb and it worked a treat !

    • @nbrworks
      @nbrworks 26 дней назад

      That's very cool! Thanks for letting me know!

  • @bmalovic
    @bmalovic Месяц назад

    Burned wood do not stink.. it smell, and it smell nicely. Not for moder "fine" noses, but ask your grandmother... I understand promotion, but.. you are someone who make parts on lathe, mill... and for you non assembling is a feature? NO it's a bug. And of course.. your modern western opsesion with safety for idiots.... Make thing that idiots can use... only idiots wil use it.

  • @mike9500
    @mike9500 Месяц назад

    🤣

  • @joem9380
    @joem9380 Месяц назад

    What kind of milling machine do you have?

  • @yousafmasih8932
    @yousafmasih8932 Месяц назад

    ❤❤❤🌹🌹🌹👍👍👍🙏🙏🙏

  • @Nathan-t6c
    @Nathan-t6c Месяц назад

    Good Jobs

  • @monkeysuncle4818
    @monkeysuncle4818 Месяц назад

    Nice work on a clean design, well worth the wait. Now looking forward to the carriage stop video.

  • @AndreLuiz-gk1mf
    @AndreLuiz-gk1mf Месяц назад

    no narrator 🙏🏼👍🏻