I Damaged my HKS RB28 Engine in my R34 GTR

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  • Опубликовано: 7 сен 2024
  • Its a sad day in the shop as we pull apart the RB28 in the GTR. In the last video I showed a clip where I mis shifted and threw a check engine light and limped the GTR back to the shop. Lets figure out what we damaged.

Комментарии • 905

  • @AdamLZ
    @AdamLZ 11 месяцев назад +4553

    Granny shifting… not double clutching like you should. Now me and the mad scientist gotta rip apart the block to fix the piston rings you fried. 🤦‍♂️

    • @PositionGain
      @PositionGain 11 месяцев назад +48

      U funny 😂😂

    • @kellinpatler
      @kellinpatler 11 месяцев назад +7

      😂😂😂😂

    • @slimsincere5015
      @slimsincere5015 11 месяцев назад +7

      😂😂😂 #DomTorrettoVc😂😂😂

    • @EL_P2Though
      @EL_P2Though 11 месяцев назад +8

      Hell nah 😭😭😂😂

    • @ism7916
      @ism7916 11 месяцев назад +74

      I'd say Adam won this comment smack down! lol classic!

  • @ALTF26
    @ALTF26 11 месяцев назад +594

    Don’t let any of this distract you from the fact that Hector is going to be running 3 Honda Civics with spoon engines, 3 T66 turbos, with NOS, and a Motec system exhaust.

  • @sputnikalgrim
    @sputnikalgrim 11 месяцев назад +893

    Leave it to TJ to wait 2 years on a build just to mess it up a week after delivery

    • @jesseortiz9007
      @jesseortiz9007 11 месяцев назад +23

      It's comical how easy it is to shift from 2nd gear to 3rd gear in these cars. I honestly laughed when it happened considering how easy it was to shift this car when I drive em.

    • @bg710
      @bg710 11 месяцев назад +28

      @@jesseortiz9007 but but but the transmission was cold 🤣🤣

    • @Crazy_CAT16
      @Crazy_CAT16 11 месяцев назад +7

      @@bg710 rookie mistake

    • @emilianofajardo9487
      @emilianofajardo9487 11 месяцев назад +9

      @@jesseortiz9007yeah but right hand drive is honestly very easy to confuse

    • @jesseortiz9007
      @jesseortiz9007 11 месяцев назад +12

      @@emilianofajardo9487 Shift pattern is exactly the same, only thing that changes is what hand you use to shift with. RHD doesn't change the gear pattern

  • @hybridevolve6759
    @hybridevolve6759 11 месяцев назад +144

    I know it’s a bad situation. But these in detail videos are the one 👌

  • @David5Suggs
    @David5Suggs 11 месяцев назад +79

    This is a really painful video, but I appreciate this type of video. You're incredibly open & honest about a shit situation and we appreciate it whole-heartedly. These videos are great none-the-less.

    • @allspooledup2584
      @allspooledup2584 11 месяцев назад +1

      Really not that painful at all if it’s just a head gasket. That’s like best case scenario

    • @fredericoespinoza
      @fredericoespinoza 11 месяцев назад

      its just more content to make more money bro shush

  • @Nick.Pellerin
    @Nick.Pellerin 11 месяцев назад +50

    7:07 His face followed by Tj's look on his face like "this is not funny" was priceless😂😂

  • @johnnybenefield5030
    @johnnybenefield5030 11 месяцев назад +61

    The reason you always take out all the spark plugs to do a compression test is which it should have showed up in your test is if it has a bad spot in-between two cylinders with the plugs in it will not show up but with all plugs out it will 99% of the time

    • @xiukn8
      @xiukn8 11 месяцев назад +4

      But compression test was still good 😂

    • @johnnybenefield5030
      @johnnybenefield5030 11 месяцев назад +2

      @@xiukn8 that is why I said 99% of the time

    • @duanebailey6253
      @duanebailey6253 11 месяцев назад +3

      The valves open and close giving an escape point. Plugs wouldn't really change that. As seen from no variance in both tests.

    • @johnnybenefield5030
      @johnnybenefield5030 11 месяцев назад +4

      @@duanebailey6253 I have been working on motors for 30 years and like I said it matters most of the time but like I said not always. It matters how bad the head gasket is blown. TJ's if you look it wasn't bad because he shut it down fast, if he kept running it would have especially when it eats a grove in the gasket.

  • @lokijones8324
    @lokijones8324 11 месяцев назад +9

    Make sure that you check piston to deck height on every piston while you have the head off. If you over revel it, had a blown head gasket, and coolant leak issue, you could have possibly bent a rod, or squished a rod bearing. Good to check now before you slap the head on.

  • @auralxtc
    @auralxtc 11 месяцев назад +18

    If you get away with just a blown head gasket, you are doing alright. Much better than a bent rod or a valve issue.

    • @duanebailey6253
      @duanebailey6253 11 месяцев назад

      I'd be more worried about the crank and bearings. Doesn't take much to upset them early on especially with added rpm/harmonics.

  • @Steu022
    @Steu022 11 месяцев назад +16

    If you remember a few episodes back during the build/tune on the car, you guys had mentioned you noticed a good amount of smoke coming from the tale pipe which could have been the start of the gasket going 🤷‍♂️

  • @TeknicZ
    @TeknicZ 11 месяцев назад +69

    Didn’t hear you say it but it would be in best interest to also replace those studs if Ian is saying those rear nuts didn’t crack when removing them then it is highly possible that they won’t torque down properly not 100% likely but it’s better safe than sorry

    • @Vitormarques542
      @Vitormarques542 11 месяцев назад +7

      probably they werent torqued right from the beginning

    • @toft5320
      @toft5320 11 месяцев назад +9

      they are not reusable to begin with and im sure these dudes know that

    • @boboso7238
      @boboso7238 11 месяцев назад +7

      Nah bro, the goat went to the goat, spent goat money to get the goat built. No way they missed a torque spec. 🐐🤣🤫

    • @boboso7238
      @boboso7238 11 месяцев назад

      @@toft5320 JB weld fixes everything.

    • @TeknicZ
      @TeknicZ 11 месяцев назад

      @@boboso7238 you ain’t lying I jb welded my drive shaft back together 4 years ago after it split in half and it’s still together vibrates a lot but it drives

  • @wbass243
    @wbass243 11 месяцев назад +5

    TJ, Also get the replacement parts that you need when you do maintenance, like main seals and any other seals that need to be flown in from Japan. You can cover each part with vasoline (assuming they are ok to be contacted with petrol )and vacuum seal them with a vacuum seal bag. then when its time to use them degrease them and clean them nicely so you have the parts on hand. Keep them away from sunlight and oxygen and they should last 10 years

  • @nickouzounian8415
    @nickouzounian8415 11 месяцев назад +36

    Bro I learned so much from this video you guys explained everything so well

  • @gorto90
    @gorto90 11 месяцев назад +1

    Honestly gotta say, very sad this happened but this is one of the MOST interesting video you ever put out, digging deep into a rb26 is really fascinating, learned alot

  • @cppctek
    @cppctek 11 месяцев назад +9

    Replace the studs. Replace the gasket. Check the deck surface for any high or low spots not just cracks

    • @thepunisher3810
      @thepunisher3810 11 месяцев назад

      Bearing clearances need to be checked amongst other things as well

  • @BrianCrofoot
    @BrianCrofoot 11 месяцев назад +2

    I’ve built a couple RB’s that are still living at high horsepower. What you should really do is deck the block and head, and use a Nitto head gasket. They are basically an O-ring style gasket that work great at high horsepower. They just need a fresh/flat surface to work properly. Also, I always set the head on the dowels and then insert/finger tight the head studs. Torque up the nuts. Start the engine and let it warm up. Dump the oil and then rip the valve covers back off and retorque the head studs after a heat cycle or three. Also, not money shifting helps a lot. Something, something mechanical sympathy. Screw that, I plan on CRUSHING on my 2.8 Nitto build. Good luck bro. Love the RB content.

    • @duanebailey6253
      @duanebailey6253 11 месяцев назад

      The smart play would have been going to a reputable builder and use what he recommends for the build. Would have been a quarter of the price and handle way more power. N1 crank with aftermarket rods and pistons for the win. No twin turbo nonsense. Way less heat and no need for low end tq in a turbo car.

    • @BrianCrofoot
      @BrianCrofoot 11 месяцев назад

      @@duanebailey6253 I agree. I’ve used the same engine builder for 2-3 RB builds, with great luck. And all of my builds, including my current Nitto 2.8 stroker have been single turbo. My new build is also going shimless bucket, which I’ve never done before, but I’m hoping I will be able to rev this bad boy to 9k rpm or higher if it’s still making power up there! Just trying to help TJ because not many people build RB’s over here yet, and they require almost no margin for error. His HKS stroker would have probably been fine if he didn’t money shift, living at ~600whp, but since it’s all apart, I would recommend doing what I said. Get it to a machine shop, get it all checked and decked, and re-torque the head again after a few heat cycles before turning up the power.

    • @Crazy_CAT16
      @Crazy_CAT16 11 месяцев назад

      It's true that it's difficult if you don't know what to ask or ask for advice on the RB engine, this is the same thing that Adam experienced when he first had an R32 sedan and he met the GDR god Andrew Hawkins
      @@BrianCrofoot

  • @Lincolnr82
    @Lincolnr82 11 месяцев назад +7

    That money shift could have caused an over-boost, lifting the head and torching the head gasket. And of course, like everyone else mentions, make sure to replace the head studs. Seems like you stretched the back ones.

  • @vickomf1
    @vickomf1 11 месяцев назад +6

    I was looking forward to this video YESTERDAY!!!

  • @johnjoseph3908
    @johnjoseph3908 11 месяцев назад +4

    not gonna lie. tj u scored big time with bringing Ethan to the team. mans a automotive monster.

  • @KingJojoB
    @KingJojoB 11 месяцев назад +184

    If you didn’t come from tiktok raise your hand 🤚🏽

  • @OGAwsomSauce
    @OGAwsomSauce 11 месяцев назад +22

    Did you guys see the chipped valve? This kind of gasket blowout is common on 10th Gen civics

    • @MichaelDrowley
      @MichaelDrowley 11 месяцев назад +3

      Yeah, can’t believe they didn’t see that.

    • @rojo9063
      @rojo9063 11 месяцев назад

      Fr

    • @jhall9936
      @jhall9936 11 месяцев назад +2

      Came looking for this comment I was like surely they noticed the chipped valve

    • @DriftNick
      @DriftNick 11 месяцев назад

      It's not chipped, just some crap on the valve.

  • @mj_aussie_coaster_travels8310
    @mj_aussie_coaster_travels8310 11 месяцев назад +2

    My moneys on that head gasket being poo since day one. The mis shift just nailed it.
    When the builder says the gaskets are crap and doesn’t replace it with a trusted brand to keep costs down on a half million dollar Datsun there’s something not quite right.

  • @martinellis3327
    @martinellis3327 11 месяцев назад +5

    I really enjoyed and appreciated you guys brainstorming and explaining what it was you were doing and seeing, from someone who loves cars but has limited mechanical knowledge, it was great!

  • @Minebiowerz
    @Minebiowerz 11 месяцев назад +1

    spaced metal head gaskets are the way to go, Turbo L series motors only last with them because the extra space allows a more forgiving combustion gap, and the metal has a lower chance of blowing out.

  • @functiongarage
    @functiongarage 11 месяцев назад +6

    Leakdown test called it on the last vid. Been through it before. Pressurize it and the air will find a way out. You probably detonated on the over rev it's alot of cylinder pressure. Glad it's only the head gasket I've had much worse outcomes.

  • @christopherharris6005
    @christopherharris6005 11 месяцев назад +1

    Awesome video as always TJ Hunt and Crew. It's going to be all good TJ. Like you always say keep moving forward.

  • @iggy_gtr
    @iggy_gtr 11 месяцев назад +7

    headlift, use the same spec studs. If you use 625 and it was torque plated with 2000s, you'll get really bad wear or scratching in the bore later on

    • @Raceman
      @Raceman 11 месяцев назад

      why this happends?

    • @iggy_gtr
      @iggy_gtr 11 месяцев назад +4

      In RB's if you machine a bore to be straight without a torque plate, and clamp the head down, the same bore that was straight prior will start to show distortion. Same issue can happen if you significantly increase clamping load on the RB if it was torque plated with a certain type of headstud. Increasing the clamping force from when it was torque plated with ARP2000 headstuds, to say ARP625, can cause changes in the bore which after some use can be visible scratching in the bore, or unusual wear in the tops of the bore.
      In this situation would be best to get a new set of the same headstuds the motor would have been machined with @@Raceman

  • @AlexDrifts
    @AlexDrifts 11 месяцев назад +3

    That is the EXACT area the block fails in Rb blocks, CHECK THE HEAD STUD GOING INTO THE BLOCK!!!! There may be slight cracks showing on side of block.
    if you magnaflux the block you should see it. CHECK THE BLOCK!!!!

  • @rozijntje
    @rozijntje 11 месяцев назад +9

    Check the valves for seal, the most common result of misshifting is actually valves touching the pistons due to very high rpms at that point.
    You might have bent a valve or two.

    • @fabini14
      @fabini14 11 месяцев назад

      Leak down test is good impossible to have bent valves.

    • @slabgizor1176
      @slabgizor1176 11 месяцев назад

      They would've known when they did a second compression test

    • @jonathanclarke452
      @jonathanclarke452 11 месяцев назад +3

      13:20 shows a broken valve

    • @fabini14
      @fabini14 11 месяцев назад

      @@jonathanclarke452You are wrong lol is just carbon on top of the valve... they have done leak down is impossible to have bad valves

    • @jonathanclarke452
      @jonathanclarke452 11 месяцев назад

      @@fabini14 lol? Chill with the big brain attitude. It might be but there’s a lighter colour gold in the crease where I think the crack is. I didn’t see the compression test so it’s just off their word. Wouldn’t doubt them trying to sell parts and be less than forthcoming about their condition publicly. Could have just been overlooked in editing. My engine has better compression numbers than this but bad leak down. Still drives fine and have run it like that for years now.

  • @mrgardner2461
    @mrgardner2461 11 месяцев назад

    I speak for everyone when I say “I’m disappointed in you” but you’re still the man.

  • @B_M_A
    @B_M_A 11 месяцев назад +37

    That's super weird that it blew the gasket. I wasn't expecting that purely because it's not common considering the circumstances. Must just be how the motor is spec'd out.

    • @slabgizor1176
      @slabgizor1176 11 месяцев назад

      I suppose because it lifted the head

    • @estebanquito356
      @estebanquito356 11 месяцев назад

      Exaclty, that engine most probably had bad timing due to the over rev, then it blew the head gasket. With only the head gasket blown it can still rev up and run, even the first compression test was ok so the car should still run. Also you can hear it miss firing evenly not only 2 cylinders.

    • @25Neo
      @25Neo 11 месяцев назад

      its actually a very common thing to happen when a head is lifted, especially considering the motor was over revved, its not like lifting a head from to much boost or not good enough head studs, as well as the head being lifted, there is so much combustion at 10-11k rpm or whatever rpm it may have revved out to, im surprised it didnt blow the head gasket worse

    • @duanebailey6253
      @duanebailey6253 11 месяцев назад +1

      This is why you always check the studs after the break in period. Things change after a few heat cycles. But even still the added harmonics from the over rev will be enough to damage things. These blocks have no bracing at all. The spoon ceo breaks it down well comparing blocks. Think it's when they rev the b16 over 11k.

  • @jaysmith2385
    @jaysmith2385 11 месяцев назад

    I have lifted a few heads on my cars. With that said. I always take the head to get inspected by the mechine shop, order new head gasket and new head studs. For the block side I visually inspect the block and put a straight edge on it to make sure it’s within spec.
    Over the years I have learned that my motors that are either o-ringed either on the head or the block are much better at not lifting heads.

  • @erichernandez1110
    @erichernandez1110 11 месяцев назад +3

    Hopefully its back up soon! Get a straight edge and feeler gauge to check the flatness of the decks, too far gone would just cook the new head gasket.

  • @Solelymotivated
    @Solelymotivated 11 месяцев назад +1

    Sorry this happened, but glad it's not too too bad of a problem for the motor!! Thanks for sharing this with us TJ!

  • @EpicBurnReturn
    @EpicBurnReturn 11 месяцев назад +25

    You need to check bearing clearances after money shifting🤑

  • @justinchapman5774
    @justinchapman5774 11 месяцев назад +37

    Look at the valve next to the blown part of the head gasket, definitely looks like a piece is broken off of it, 13:22

    • @rivalspec1210
      @rivalspec1210 11 месяцев назад +3

      Could be just dirt, the compression test would have shown low compression

    • @Crazy_CAT16
      @Crazy_CAT16 11 месяцев назад +2

      it's the coating on the head gasket

    • @GramSnax
      @GramSnax 11 месяцев назад

      solid eyes, that absolutely looks like its potentially chipped

    • @MichaelDrowley
      @MichaelDrowley 11 месяцев назад

      Also spotted this, The valve is gonskies

    • @nathanthecarguy4852
      @nathanthecarguy4852 11 месяцев назад

      Bro it looks like grease of carbon build up

  • @kylenewberry8598
    @kylenewberry8598 11 месяцев назад +34

    Didn't tommy say the headgasket was sketch when he was building anyway?

    • @hawaiian_judge5113
      @hawaiian_judge5113 11 месяцев назад +6

      yarrrr

    • @171JUSTIN
      @171JUSTIN 11 месяцев назад +1

      How so? And why use it if the builder admits it's sketch?

    • @kylenewberry8598
      @kylenewberry8598 11 месяцев назад +2

      @@171JUSTIN basically said that by design the gaskets can leak, but they don't usually give problems. But if they do, just replace them, but saves money in the initial build.

    • @Aintchuhurd
      @Aintchuhurd 11 месяцев назад +13

      Tommy is sketch

    • @Coyoteluvr
      @Coyoteluvr 11 месяцев назад +4

      That engine was fk from the moment he started it. Ity smoked so much. I think that Tommy might made a mistake.

  • @Supra_Mickey
    @Supra_Mickey 11 месяцев назад +2

    Definitely would recommend the OTC compression and cylinder leakage tester

  • @Aerospacegod
    @Aerospacegod 11 месяцев назад +9

    Im kinda shocked that the transmission doesnt have a first gear lockout. Maybe it's a possible change that can be made? I'm not sure at all just throwing it out there.

    • @MrHughk1
      @MrHughk1 11 месяцев назад

      Its a manual gearbox, MANUAL ie its not an automatic so no it does not have a first gear lock out. Could it be done with a computer and numatics, of course but then you would just automate the shift fully and you have an automatic gearbox. The point is that it takes a certain level of skill to use the manual and that is part of the attraction to master the fast 1/4 or lap. TJ just fucked up here showing off his huge wallet.

    • @yourdaddy9622
      @yourdaddy9622 11 месяцев назад +8

      @@MrHughk1you obviously don’t drive a manual buddy, they have had first and reverse lockouts for almost two decades. Maybe don’t cut someone down when you have no idea what you’re talking about. Having5 or 6 gears and a lock out of 1st doesn’t “basically make it an automatic”, you just don’t have a permit yet so are going off of video games.

    • @MrHughk1
      @MrHughk1 11 месяцев назад

      @@yourdaddy9622 Reverse yes, first is pointless even if it has been done as if you do one you need to do all as you are de skilling the driver, which makes it basically half way to being an automatic, only a clutch actuator is then required. Dont be so presumptuous yourself, im 56, got a degree in mechanical eng and work on cars and bikes for fun. And remember we are talking about early 90's tech before people catered for the lowest achiever at the expense of everyone else. Getting an award just for turning up breeds idiots like you and the commenter.

    • @duanebailey6253
      @duanebailey6253 11 месяцев назад

      ​@@yourdaddy9622normally done on the shifter. It's a pain in the butt for a street car though.

    • @yourdaddy9622
      @yourdaddy9622 11 месяцев назад

      @@duanebailey6253 like as much of a pain as literally changing every bolt on the car? You know, like he did with Tommy… yikes

  • @IxtheDuckyxI
    @IxtheDuckyxI 11 месяцев назад +1

    You sound defeated in this video I'm sorry to hear. As a fellow GTR owner I can tell you they will always give you problems lucky you have lots of money to fix this

    • @mac_19
      @mac_19 11 месяцев назад

      What kind of problems? Can you describe

  • @johnathanromero3944
    @johnathanromero3944 11 месяцев назад +22

    Blows my mind just how little TJ knows about cars…. Truly mind blowing! 🤦🏼‍♂️

    • @wotceseriescollector
      @wotceseriescollector 11 месяцев назад +3

      agreed

    • @2jyeti909
      @2jyeti909 11 месяцев назад +11

      Could be worse. Could be DDE.

    • @SUp3RpooP3r7698
      @SUp3RpooP3r7698 11 месяцев назад +4

      Well, I mean these guys aren't mechanics. They're RUclipsrs with money. I mean, I'm sure they know their fair share. But that's why they hire other people to work on their cars

    • @Justinhomii
      @Justinhomii 11 месяцев назад

      Too busy putting rivets in widebody's to learn about engines

    • @chrisdef15
      @chrisdef15 11 месяцев назад +1

      What did you expect? As others said he’s a youtuber. But from your comment he still probably knows more than you. You just criticised without giving any advice.
      2 guys who do know. 3 if you count tommy took a while to figure it out. But I’m sure you know more.

  • @jaimemedina4923
    @jaimemedina4923 11 месяцев назад +1

    Please take care of this car it’s a dream for most of us :)

  • @MrMinemadness
    @MrMinemadness 11 месяцев назад +4

    Sounds like the headstuds weren't retorqued after a some heat cycles to me.

  • @MrImhighoffmusic
    @MrImhighoffmusic 11 месяцев назад

    It's never a dull moment with calvin i swear to god. "It's ENCHANTED."

  • @halfbloodentertainment
    @halfbloodentertainment 11 месяцев назад +13

    Woah what happened ? Didn’t I watch this yesterday 🤣 either way, poor FineSpec😭 we praying for y’all🙏🏼

    • @adamportman9084
      @adamportman9084 11 месяцев назад

      i was triple out

    • @adamportman9084
      @adamportman9084 11 месяцев назад

      trippin

    • @MrSelmo85
      @MrSelmo85 11 месяцев назад +3

      When i tried to watch it yesterday it was set to private.. something was likley cut..

  • @ultimatespartan6244
    @ultimatespartan6244 11 месяцев назад +1

    when you striped the motor the first time was there not already a blow head gasket - and when you guys assemble it did the measure the block and inspected in-between the a straight edge and a feeler gauge or did you just assembled it before assembling this engine please measure and do a die test on the block as well by dyeing the block and taking a marble counter top that is straight and run it back and forth to take the die of and if all the die comes of its right but if there is still die on between the cylinders then you now you have a low spot as well check on the head of any low/high spots you can check by just you're eyes

  • @gregcass12
    @gregcass12 11 месяцев назад +173

    Imagine paying $70k for a motor then money shifting 😂

    • @JoshQc
      @JoshQc 11 месяцев назад +23

      He payed more than 70k buddy, over 100k

    • @wotceseriescollector
      @wotceseriescollector 11 месяцев назад +14

      he will keep making vids until it pays for it

    • @loan-shark
      @loan-shark 11 месяцев назад +30

      he's a millionaire - this is content.. wish i had a staff working on my cars while earning money 😂

    • @boboso7238
      @boboso7238 11 месяцев назад +9

      The S2000 has more than $100K under that hood. The Skyline easily has more than that in labor and anodized colored parts, Tommy got to get paaaaiiid.🤣

    • @JDMz
      @JDMz 11 месяцев назад +4

      ​@@JoshQche paid 100k in just exterior mods let alone the engine 👁👄👁

  • @alexstava
    @alexstava 11 месяцев назад

    Bruh, I wasn't expecting that the first compression test was done incorrectly, Tommy knows how it should be done

  • @kontrix1
    @kontrix1 11 месяцев назад +11

    13:20 you have a broken valve as well

    • @kopyking37
      @kopyking37 11 месяцев назад

      Saw that too

    • @Crazy_CAT16
      @Crazy_CAT16 11 месяцев назад

      it looks like it's the coating on the head gasket

    • @justinchapman5774
      @justinchapman5774 11 месяцев назад +1

      Definitely looks like a piece of the valve is missing, definitely look at the valve next to where the head gasket blew, it may just be carbon but even zoomed in on looks broken

    • @DylanTK
      @DylanTK 11 месяцев назад +1

      yep, and that's exactly what lifted the head

    • @MichaelDrowley
      @MichaelDrowley 11 месяцев назад

      Yep

  • @iswinkels
    @iswinkels 11 месяцев назад +1

    Don't use that copper spray crap on the head gasket when you assemble next. Use ACL Hylomer spray instead. Copper spray is more suited to o-ringed/copper head gasket setups. All the JDM gaskets were originally meant to be installed dry.
    Also depending on the head stud and tension your running, there is a mod you can do to the head to prevent the head stud hole from collapsing under the washer and nut. A workshop with a CNC mill can machine out the tops of the head stud holes, and then you press in ARP1/2" insert washers with a 0.001" press fit. This prevents the head stud hole crushing, and stops studs going loose.
    A re-torque may have also prevented this, so consider doing that after the first few heat cycles before you give the rebuilt engine a hard time.

    • @Xolition
      @Xolition 11 месяцев назад

      You sound like you've done this before!

  • @sarahm3881
    @sarahm3881 11 месяцев назад +10

    My Toyota Camry would neverrrr 😂

    • @ND-ICU
      @ND-ICU 11 месяцев назад

      My Camry Blew the a head gasket first then Blew the Engine a couple months later 😂😂😭😭😭

  • @jaycemoore12
    @jaycemoore12 11 месяцев назад +1

    Fun to see you guy’s diagnose the car loved the video! Sucks you money shifted but everything’s fixable brotha can’t wait to see her on the road again

  • @2jyeti909
    @2jyeti909 11 месяцев назад +4

    So i guess this means adam has the better R34 GTR 😂

  • @GermanEliteTuning
    @GermanEliteTuning 11 месяцев назад +1

    Hug bummer but the issue could have been way worse. The Bloopers were great. You should bring them back in every vid 🤘🏻🤘🏻

  • @spliff08
    @spliff08 11 месяцев назад +6

    TJ bricked his $100,000 car 😂

    • @deanwilson9317
      @deanwilson9317 11 месяцев назад +4

      If I had to guess $100,000 is an understatement…

    • @drewole
      @drewole 11 месяцев назад +1

      Bro, thats worth way more than 100k

    • @connoisseuroftigolbitts
      @connoisseuroftigolbitts 11 месяцев назад +1

      Try more like $250k +

    • @johnathanromero3944
      @johnathanromero3944 11 месяцев назад +2

      He could brick a $5 car or a $1,000,000 car… it’s TJ, he’s got ZERO clues about cars and it shows in every video…. One of the reasons I watch it is to get a laugh at someone “so accomplished” in racing and cars knows absolutely NOTHING about cars and can only read a script and not a repair manual…. Sad

  • @HellcatDreaminJosh
    @HellcatDreaminJosh 11 месяцев назад

    TJ Hunt Great Video I'm glad your R34 GTR Skylines engine is fixed and I hope you don’t miss shift again

  • @Dirtyz1234
    @Dirtyz1234 11 месяцев назад +3

    Did you even hose the gasket down with copper spray and say "that ain't goin nowhere" 😅

  • @nozzomeister844
    @nozzomeister844 11 месяцев назад +2

    Anyone else see the teased R34 GTT left rear quarter in the end of the video when he puts the hand over the camera! New project?!

  • @lIlIllll1
    @lIlIllll1 11 месяцев назад +4

    Thats why u can't trust tommy to build shii

    • @kulvircheema955
      @kulvircheema955 11 месяцев назад

      I totally agree with you

    • @Crazy_CAT16
      @Crazy_CAT16 11 месяцев назад

      That's why Adam's engine setup on the R32 is very different from the build that Tommy usually does, that's what Tommy talks about in his video.

  • @phosimmie
    @phosimmie 11 месяцев назад +2

    Who else was able to watch yesterday? Noti Gang!

  • @Jyuaa
    @Jyuaa 11 месяцев назад +3

    Hey TJ hope everything goes well brother 👍🏽

  • @KableTac
    @KableTac 11 месяцев назад +2

    pretty standard feature for every tommy spec engine.

  • @chiva4life17
    @chiva4life17 11 месяцев назад +3

    Anyone catch that yellow R33 sneak peek at 14:28 lol?

  • @thejasonstackhouse
    @thejasonstackhouse 11 месяцев назад +1

    Surely I'm not the only one who saw that the intake valve below Tommies finger at 13:42 is broken and has a clear chip in it.

    • @thejasonstackhouse
      @thejasonstackhouse 11 месяцев назад +1

      1000% broken valve on intake cylinder 4. I just zoomed the video in to make sure it wasn't grease or something dark sitting on the valve, it's not I can clearly see the metal is sheared

  • @dennnster
    @dennnster 11 месяцев назад +6

    Hi TJ. So when are you getting a NSX? ;) Love the content!!

  • @PinkuStyle
    @PinkuStyle 11 месяцев назад

    All good champ it happens. Ive had a good run with RBs. Many years also broken some. We drive them it will happen. See ya at Laguna. Ps
    You can rotate the engine with the alternator or power steering pulley.
    The compression test wws definitely wrong. Best is testers in each cylinder one shot and done and or all plugs out, fuel disconnect (cas plug) WOT test.

  • @chrissantana6688
    @chrissantana6688 11 месяцев назад +5

    why'd you take down the video from yesterday, did you not want people to see the yellow r34 in the background that may be the next giveaway car or that tommy is coming down to help and do another project?

    • @ColinRay999
      @ColinRay999 11 месяцев назад

      Awfully specific comment lol

  • @BNR_248
    @BNR_248 11 месяцев назад

    I find it strange it stretched a head just from a slight money shift that was caught early. I reckon those headstuds werent torqued to yield, the moneyshift just revealed an underlying issue and took the already damaged headgasket with it. High Cylinder pressure or incorrectly torqued studs stretches head, revving to eleventy off boost would hurt the pump, bearings, shims, valves, timing etc... none of which were damaged as far as we know.

  • @Wynaut1517
    @Wynaut1517 11 месяцев назад +1

    Love the bloopers. Pray the R34 gets fixed soon!

  • @haydencrews7009
    @haydencrews7009 11 месяцев назад

    Yes everything that you are seeing is exactly how my truck went, no cracked head or anything. Our gaskets look the same straight blowout between 4 and 5

  • @MattMatt77
    @MattMatt77 11 месяцев назад +2

    Happy to see it finally Uploaded. Because yesterday was taken down.
    But because everybody knows more about cars than me and because I'm wrong why is it such a big deal if you shift into a wrong gear why would that hurt the engine?
    I would likely get a copy and paste reply from Google😂🤣💀

    • @IAmPyrofan
      @IAmPyrofan 11 месяцев назад

      I know very little. But just from watching car channels. You shouldn't redline the engine. And when you shift down into a lower gear when you meant to go higher, the rpms are going to spike and more than likely rip past the redline. Which can cause the problems shown and explained in the video.

    • @MattMatt77
      @MattMatt77 11 месяцев назад

      @@IAmPyrofan Well what happens is that if you go from let's say 2gear back back in to 1gear. Let's say redline is 5k. You would be at maybe/likely 11k rpms in 1gear. That would put crazy high stress on every single part of the car Engine and transmission side.
      So over all it's very bad. This is also why I only like automatic cars. Because I have a hard time seeing what gear I'm gonna go in if it's not a gated shifter. I do know how to drive manual I also have manual bikes. But to me it's a lot easier because you don't have mistakes like this.
      But that's coming from a person like me that's on the spectrum so somebody can easily argue and say that I'm wrong because I'm not good at arguing 😑

  • @010720
    @010720 11 месяцев назад

    Clean the block surface and run a straight on the deck to make it’s not warped same for the head surface, and new head studs for sure and check the block head studs holes make sure the back ones aren’t messed up

  • @thomasmacintyre3768
    @thomasmacintyre3768 11 месяцев назад

    it makes me happy seeing another Thomas doing well

  • @__jacob
    @__jacob 11 месяцев назад +2

    YELLOW R34?! I see you

  • @paschen129
    @paschen129 11 месяцев назад

    The engine of that car was really special. (Nismo Fine Spec Final Edition RB26DETT) Installing an HKS stroker kit is the biggest betrayal of that engine and it's really sad that this happened.

  • @XoliQCX
    @XoliQCX 11 месяцев назад +1

    If you look at 13:26 there is what is looking like a burnt/broken exhaust valve

  • @evanmlevy
    @evanmlevy 11 месяцев назад +1

    Crazy I thought you posted this yesterday but couldn’t find it!

  • @twelevensies
    @twelevensies 11 месяцев назад +1

    I feel for you TJ, but this is interesting and informative content so at least there is that.

  • @ZayP9
    @ZayP9 11 месяцев назад

    At least your blessed enough to have a US legal R34 GTR to money shift!

  • @johny79action
    @johny79action 11 месяцев назад

    Every compression test should be done with all plugs out throttle wide open, hopefully you got lucky and the gasket is the only issue.

  • @BoostedSpeedDemon
    @BoostedSpeedDemon 11 месяцев назад +2

    How did nobody notice the big chunk missing out of the valve by the head gasket failure? 13:21

    • @DriftNick
      @DriftNick 11 месяцев назад

      It's just some crap on the valve.

  • @BattlingWarrior1985
    @BattlingWarrior1985 11 месяцев назад +2

    So glad it was just the gasket and that you didn't have to buy a whole new head or block

  • @scuffedgravyboat
    @scuffedgravyboat 11 месяцев назад

    whatever that medieval bit y’all were doing was hilarious

  • @walther89
    @walther89 11 месяцев назад +1

    Fly Josh out.... or not but damn unlucky, dont be that excited to shift, just chill :)

  • @vz358
    @vz358 11 месяцев назад +1

    TJ give your guys the credit they deserve... stop saying "WE" when you're not even they're helping.

  • @95turbostang21
    @95turbostang21 11 месяцев назад

    Taking all of the spark plugs out and doing a compression test, all it is going to do is have a little more higher PSI because the motor's turning quicker, that's it either way is fine.

  • @Team6Loves
    @Team6Loves 11 месяцев назад

    TJ, welcome to RB26 ownership.
    I did this exact same thing to my GTR-33 and my GTR-32.

  • @___joez
    @___joez 11 месяцев назад +1

    The video summary is about a car enthusiast who experienced engine problems with his car, a Nissan R34, while giving a ride to a fan. The car went into a limp mode due to a misshift, and they attempted various diagnostic steps, including checking spark plugs, compression, and timing. They also performed a compression test but couldn't find a clear solution.
    They suspected a head gasket issue, and upon further inspection, they found evidence of a blown head gasket. Additionally, there was rust on the valves, indicating coolant contamination. The video ends with the plan to replace the head gasket and get the car back on the road.
    In summary, the video discusses diagnosing and identifying a blown head gasket in a Nissan R34 due to engine performance issues.

    • @the.villan
      @the.villan 11 месяцев назад +1

      Thank you ChatGPT

    • @johnathanromero3944
      @johnathanromero3944 11 месяцев назад

      Explain the “engine performance” cause.. it was a junk head gasket to start with and it did the engine builder figured it would. Hard lesson to learn but on big boy toys….YOU NEVER PUT SKTECH PARTS IN! It’s ok, TJ has $$$ and people to fix his problems like usual lol

  • @yourdaddy9622
    @yourdaddy9622 11 месяцев назад

    TJ you can easily fix this problem.
    Just go 1,2,3,4… but it has to be in that order.
    All jokes, your hood is worth more than my car.

  • @Juan_More_Mile
    @Juan_More_Mile 11 месяцев назад

    Love Ian not taking Tommy's bullshit when his pinky has more mechanical knowledge

  • @mattevans3212
    @mattevans3212 11 месяцев назад

    Im sorry that happened to your new car Teg, i know how disappointing it is to just get a car on the road and have it buggered in a couple of weeks lucky you have a mad crew.

  • @MechanicalMafioso
    @MechanicalMafioso 11 месяцев назад

    Like Cletus said, they make more money blowing up engines than just running. Blown engine = drama, drama = $$$ 🤷‍♂️

  • @3rdPedalMedia
    @3rdPedalMedia 11 месяцев назад

    put a pressure sensor in your coolant plumbing, setup setup a warning and shutdown in the haltech i believe over 40psi? double check this. but this would tell you about head lift

  • @brandonbdl
    @brandonbdl 11 месяцев назад

    10:08 this was straight up a skit out of a movie 😂😂 Dylan voice is on point. 😂 this dude is absolutely awesome !

  • @duanebailey6253
    @duanebailey6253 11 месяцев назад +1

    Check the oil. Sounds like a spun bearing. It will go away and come back. Engine didnt sound right and knocking in certain points.

  • @DesperadoGarageOfficial
    @DesperadoGarageOfficial 11 месяцев назад

    The Windows XP shutdown 😂😂😂😂. I completely lost it

  • @oohhhdaniel
    @oohhhdaniel 11 месяцев назад

    I money shifted my Focus RS like 2 years ago. I think (hope) some wizardry in the software saved me and prevented things from getting destroyed like this. I guess one day I’ll rip the engine apart and find out. I definitely know that feeling immediately after it happens though.

  • @brandonclark2170
    @brandonclark2170 11 месяцев назад

    I remember when this video went up yesterday and the yellow car was blurred out in the background. Good times lol

  • @calvinchau6873
    @calvinchau6873 11 месяцев назад +1

    RB26 problems. Thank God for the 2JZ

  • @nikkoboyd1998
    @nikkoboyd1998 11 месяцев назад

    Sweet man, no big deal. Get her done.