Комментарии •

  • @celtos255
    @celtos255 3 года назад +56

    i was waiting for that whole carport to come crashing down

    • @davew1584
      @davew1584 3 года назад +2

      Haha yeah I was the same.

    • @VSTV1993
      @VSTV1993 3 года назад

      Thought exactly the same

  • @TheTechnoaddict
    @TheTechnoaddict 3 года назад +21

    "I'm just a diy mechanic"!. The dept of your videos and the stuff you do go's beyond what most mechanics know about cars! The only difference is they have a computer that says wich bolt to take out in the right order😁. Coffee and this in the morning is just perfect!

  • @Showing_the_car_
    @Showing_the_car_ 3 года назад +32

    05:17 "Everything on it is just awkward" - my thoughts exactly of Fords! Then I got a BMW and found out what awkward really means. Keep up the good work Steve!

    • @Stop..carry-on
      @Stop..carry-on 3 года назад +3

      I think bmw start the design process from the common parts that need replacing and build a car around them - with plenty of plastic clips that snap off

    • @Showing_the_car_
      @Showing_the_car_ 3 года назад

      @@Stop..carry-on Yep, and every clip is a different design.

    • @anthonynewcome128
      @anthonynewcome128 3 года назад +1

      try a mk1 TT. the factory techs must have the hands of 5 year olds

    • @barnabasmolnar7598
      @barnabasmolnar7598 2 года назад

      This is why I have a suzuki swift/cultus :"D cheap and idiots can work on it as well (including myself).

  • @karls9311
    @karls9311 3 года назад +26

    Could make a nice coffee table out of the old block Steve!

  • @c3dpo
    @c3dpo 3 года назад +19

    My kind of DIYer with a whole front end dismantled 🍻

  • @thereviewer7931
    @thereviewer7931 3 года назад +139

    Who else Is up enjoying some spark plug Steve? 😅

    • @warwickscram5925
      @warwickscram5925 3 года назад +5

      I was just about to go to sleep but I love to see blown up engines.

    • @Alexander_l322
      @Alexander_l322 3 года назад +4

      @@warwickscram5925 if it’s someone else’s I don’t mind 🤣

    • @chrisvectra5296
      @chrisvectra5296 3 года назад +1

      I’m here watching
      Why did the engine let
      Go
      Too much boost dodgy tune?

    • @jasonwalkley53
      @jasonwalkley53 3 года назад +1

      He's a genuine petrolhead just like the rest of us ..it's like someone has died in the family!! Just think of that m egane m8..you was all over him like a rash..that's how quick Steve's car was..Fast Fords..Steve best of luck with rebuild fella110%.☆

    • @alan4391
      @alan4391 3 года назад

      Yea that engine is toast 👌

  • @warwickscram5925
    @warwickscram5925 3 года назад +33

    ALLOE YOO TOOB

  • @traptrix7621
    @traptrix7621 3 года назад +5

    Everyday we learn something new is a good day. I know more than I did before I watched this. Thank you!

  • @Alexander_l322
    @Alexander_l322 3 года назад +8

    Nice to see it apart and confirmed the rings are reason. A few of us said it was the rings. no speculation as to why but I have a suspicion. I’ll be glued for the next one Steve.

  • @chrisyoung5573
    @chrisyoung5573 3 года назад +2

    Great video Steve, gone are the days you carry a box of spanners in the boot in case you break down while out. The modern engine is so complicated now. Your doing far better than i would

  • @markcrowley7042
    @markcrowley7042 3 года назад +2

    Cracking video, good to see you still smiling 😀 can’t wait to see the rebuild and you back on the track 🚙

  • @peterlobb6456
    @peterlobb6456 3 года назад +1

    Great job and I'm glad that all the damage seems to have occurred below the piston crown and the turbo didn't get damaged (hopefully). I can't believe how much stuff there is to strip down just to get the head off of a modern engine !

  • @jameswilson8820
    @jameswilson8820 3 года назад +6

    The joys of chasing power😁upwards and onwards Steve👍😁

  • @reggiedixon2
    @reggiedixon2 3 года назад +5

    Great video Steve, very informative. There is nothing like actually doing the post mortem.

  • @wurlyone4685
    @wurlyone4685 3 года назад +1

    Well done getting it apart, interesting to see the results.
    One step closer to having it back one the track 👍

  • @garethedwards2883
    @garethedwards2883 3 года назад +1

    Thanks so much Steve for taking the time to strip the engine to see what the failure was even though like you say the piston rings from cylinder 1 have dis-integrated. Also don't explain to your followers about your skill level as you should give yourself credit as you are willing to give anything a go and are very competent.

  • @Adam151082
    @Adam151082 3 года назад +6

    Good luck with the rebuild Steve, good to see you having a go yourself.
    Ps. I love the sound of the rain hitting your car port 😍👌🏼

    • @Sparkplugsteve
      @Sparkplugsteve 3 года назад

      Hey thanks Adam and good luck with the garage build. Iv been watching 😁 not at all jealous lol

  • @davidandrews5510
    @davidandrews5510 3 года назад +16

    I think it’s fair to say Steve ... that car keeps u busy

  • @Triicks111
    @Triicks111 3 года назад +2

    Excited for more videos from you Steve, this is really interesting!

  • @Pu1gcerda1
    @Pu1gcerda1 3 года назад +7

    Hi Steve, I know it is a sad subject, but ironically I think this is one of your best videos
    Keep safe

  • @Harrisoncardiff
    @Harrisoncardiff 3 года назад +1

    Love your stuff steve hopefully get it all sorted soon, love the vids and personality🏴󠁧󠁢󠁷󠁬󠁳󠁿

  • @Ford84
    @Ford84 3 года назад

    Nice little video to wake up to! Good job getting it stripped down Steve, we all knew it but we all had to see it! 😂😂 looking forward to the replacement engine install! 👌🏻

  • @davew1584
    @davew1584 3 года назад

    Keep up the good work n vids Steve. Can’t wait to see this back up and running.

  • @jmp4285
    @jmp4285 3 года назад

    Thanks for the great video again and especially when you share this experience.You have a big job up front again so good luck. 👍

  • @si.cp4457
    @si.cp4457 3 года назад +1

    Unlucky dude hope you get it sorted and back up and running asap I thought mine was a gonner when I blew my head gasket at cadwell Park back in November last year.

  • @gothikia
    @gothikia 3 года назад

    Great job pulling that engine out. I never considered using a pully on some timber beams before. Will have to build something up and give that a go I think for when I swap mine out.

  • @SuperBigboi18
    @SuperBigboi18 3 года назад +6

    Hope you enjoyed your cuppa well deserved

  • @stegradon7827
    @stegradon7827 3 года назад

    Nice one. Can't beat a bit of forensic analysis

  • @chrishull4174
    @chrishull4174 3 года назад +4

    Hi Steve , my theory to the problem lays in the block or the serviceability of the head gasket. Situation you have is ,the engine had wear before you started using it for track. Now I haven’t followed many of your videos but I hazard a guess that with that flash turbo its above standard tune and running higher boost / power. The more performance you run the less reliability you will have . I don’t see there was anything wrong with the the tune of the engine as everything was running fine, it’s not detonation as this happens within the combustion chamber and there’s no damage to the face of the piston. You noticed a crack in the wall of cylinder 4 liner that is your clue . compression has squeezed passed the liner either through the head gasket or coolant gallery. Possibly in turn this may have caused a air lock and a coolant restriction in the engine, when this happens coolant doesn’t flow as it should and temperature rises rapidly causing hot spots on the cylinder walls. for it to damage rings and ring lands to fail . It can be repaired but as you guess it’s just as cheap to slap in another engine and have more fun 🤩

  • @stuartdavison8459
    @stuartdavison8459 3 года назад

    Great video Steve my kind of diy mechanic love the content looking forward to the next one stay safe mate 👍 🍺

  • @timmywatkins1702
    @timmywatkins1702 3 года назад

    So easy to watch, keep them coming!!

  • @TheGazza636
    @TheGazza636 3 года назад

    wow you done a good job on that old engine.it did you well around castle coombe.look forward to see how the new engine compares when it up to doing a track day

  • @timfenton5153
    @timfenton5153 3 года назад

    Stay positive and keep going. Thanks

  • @TheGazza636
    @TheGazza636 3 года назад

    lots of useful info gained there for the future i would say steve.will all help putting the new engine back in,great video by the way

  • @Rampage686
    @Rampage686 3 года назад

    Great vid Steve! Good to see it stripped down

  • @jakemason9436
    @jakemason9436 3 года назад +7

    Thanks Steve Relaxing vid. Teardown and rain.

  • @waynelittle5583
    @waynelittle5583 3 года назад

    Great work and an amazing attitude to it onwards and upwards for yobo 🤙🤙

  • @leonstry
    @leonstry 3 года назад

    Nice Video Steve this has just happened to my son’s ST180 so when i get back to the UK from work i have to strip and rebuild his engine and this video has gave me a good few tip’s.

    • @Sparkplugsteve
      @Sparkplugsteve 3 года назад

      Sad news hope you get it sorted and thanks.

  • @jawdinker554
    @jawdinker554 3 года назад +1

    Nice content Steve thank you👍.
    When things in life go wrong i try to focus on the positive. Things happen for a reason maybe the next lap of the track if the engine blow could of been a disaster?? Keep ya chin up Steve you will be back behind Yobo's wheel soon😉👍👍👍.

  • @thomasmorgan1574
    @thomasmorgan1574 3 года назад +1

    Really enjoying the content, great work mate

  • @kamilozw86
    @kamilozw86 3 года назад +1

    Good luck with new engine

  • @marknewman6037
    @marknewman6037 3 года назад

    Aaahhhh, the Welsh engine hoist support beams. Keeping a smile on my face just after my knee op................

  • @NathanHiley
    @NathanHiley 3 года назад +2

    Keep positive Steve you’ll have it back on the road in no time 💪🏻💪🏻

  • @Ffish69
    @Ffish69 3 года назад +2

    If you're looking to get rid of parts, I really fancy one of those pulley wheels as a paperweight!

  • @olihaub
    @olihaub 3 года назад

    Another great video. Regarding the turbo my experience with popped motors and turbo is the metal fragments in the oil go through the turbo bearings and destroy them. Rarely will a bit of ring land make ot past the valves and smash the exhaust wheel.

  • @MrZimmaframe
    @MrZimmaframe 3 года назад

    Life ain't so bad, it's just a car and bits can be replaced. I hope you had some good tea Steve, all the best to you and the family.

    • @Sparkplugsteve
      @Sparkplugsteve 3 года назад +1

      Your exactly right. Iv got a good life and family and it's just a car. Thank👍

  • @terryansell9573
    @terryansell9573 3 года назад +6

    Great attitude Steve, go in have shower then go shopping for some tea and forget about it 👍

  • @richardsedorski1206
    @richardsedorski1206 3 года назад +1

    Well done sir must heartbreaking to see that piston keep up good work.👍👍👍

  • @opulent_bedbug
    @opulent_bedbug 3 года назад +2

    You give us all hope!

  • @nickmackenzie703
    @nickmackenzie703 3 года назад +1

    Great job Steve

  • @ExderFury
    @ExderFury 3 года назад

    Replaced mine this week too and i can tell you setting timeing on those is a nightmare have done it 2 times now
    First when i blew a hole in Zylinder 4 and when i replaced the engine fully
    Both times check engine light came on and i needed to get the car to ford
    Because of the tools from amazon i got

  • @gregconboy8029
    @gregconboy8029 3 года назад

    Looks like its been knocking to me. When the new engine goes in monitor the afr readings. Ideally it wants checking with a knock monitor too

  • @andrewterry1801
    @andrewterry1801 3 года назад

    Great video mate , keep up good work 💪

  • @brianthetrain9283
    @brianthetrain9283 3 года назад +4

    Keep um coming Boyo👍

  • @loomesy77
    @loomesy77 3 года назад +2

    Certainly looks like it's been hot in no.1 ring land failure is common issue with heat. Without logging afr we don't know what the ratio was but I bet it would help running it a few points richer to help with cylinder temps. Perhaps when you get the new engine filling down the ring gap a few thou to help prevent the rings butting up again.

  • @LewisGTR1997
    @LewisGTR1997 3 года назад

    Great vid Steve, was a good watch!

  • @steveguest8028
    @steveguest8028 3 года назад +11

    I thought that was what had happened, massive amount of work involved to get to the piston, you need to find out the cause otherwise it will kill your replacement engine as well, probably down to detonation/tune .... best of luck with it Steve 👍

    • @SB-vb8ch
      @SB-vb8ch 3 года назад +1

      Not enough ring gap for the cylinder pressure (boost). Absolutely text book failure.

  • @dhlcomputers
    @dhlcomputers 3 года назад +5

    Hi Steve, I was so waiting for you to say at the end of the video it's going "In The Bin!" 😎 that would have be so funny, don't know if you watch Mighty Car Mods but well done on all the hard work. I am a diyer myself.

  • @midlifecrisis9269
    @midlifecrisis9269 3 года назад

    Great vid Steve. I’m no expert but I would say thats temp related, ring failure led to the piston going. I spose it could be rebuilt but as you said, get another motor. Well done on the strip down

  • @mikej857
    @mikej857 3 года назад

    Great video Steve
    Well at least we know those who diagnosed a ringland failure were correct.
    The mark on the piston looks like it's got very hot, surprised there was no damage to the bore.
    Whats also concerning is the crack in piston 4, there's no saying this wasn't done before the piston failure and the engine wasn't showing any signs of a crack, I'm not sure as said if adding shims to the liners would solve this as you'd then be comprising the cooling between the bores and as the cut out isn't the full width like the 5 pot volvo engine would it really stop a crack from forming

  • @CookRacingUK
    @CookRacingUK 3 года назад

    All that effort.... is really appreciated Steve! Fascinating to see the scene or the crime.
    I need to take our dv6 engine out of our mark 6 Fiesta. Glow plug snapped but needs a new timing belt and clutch anyway. Looks like the front comes off quite easy. Any top tips?

  • @dnbtrooper
    @dnbtrooper 3 года назад

    You are a mechanic steve very knowledgeable..
    It got to hot!.. more than lickly head gasket gone, water mixes with oil in no1 cylinder heats up hotter than hell melted off piston ring, I melted a piston rod clean off on my old Escort mk4 Rs due to trying to keep with porsche Carrera lol, I managed to rebuild it my self head skimmed new gaskets second hand piston new rings, and shells, bearings.. ready to fight another day.
    I've got to do my timing belt soon on my Mk7 st, I'd like to see you make video for some pointers. 👍🏼

  • @pilotspadge5690
    @pilotspadge5690 2 года назад

    To say you’re not a mechanic you’re very knowledgeable, I’ve been looking for a vacuum leak for days on my Fiesta but scared to even take anything apart 🤣

  • @ThePianoCentre
    @ThePianoCentre 3 года назад

    Thanks Steve , found your video very interesting

  • @johnrowell942
    @johnrowell942 3 года назад

    Great video and hope someone can answer the reason number piston failed in that area. Take care

  • @lukewatts3284
    @lukewatts3284 3 года назад

    Mate I wish I was as confident as you! I will just take it apart 😂

  • @iainwebber-james7641
    @iainwebber-james7641 3 года назад +1

    Top video Steve keep it up👌👌

  • @Nashy027
    @Nashy027 3 года назад

    Good work Steve

  • @euanrobert6171
    @euanrobert6171 3 года назад

    Scary but fascinating amount of Piston ring on that sump bung steve

  • @jonah406
    @jonah406 3 года назад

    Just found this video, and I feel your pain. My Focus ST also suffered engine failure, 5 weeks after warranty expired. Managed to bet a goodwill gesture from Ford, but still costing me a bit. I'm thinking I may have had the same issue, as breakdown man discovered a lack of oil, will be demanding full autopsy from Ford as to what issue is,

  • @mkdundee4785
    @mkdundee4785 3 года назад

    I’m sure you can use the 1.5 closed deck block from a Cmax with 16v head from the st180

  • @blueballs_m135i8
    @blueballs_m135i8 3 года назад

    elbows deep in there Steve mate. My view is bad map has done it in simple as mate I am sure you will have back up and running soon.

  • @simonbussey7530
    @simonbussey7530 3 года назад

    Great video and a fascinating watch.
    The big question: When you install the new engine are you going to run with the same tune?!

  • @crypticmammoth9603
    @crypticmammoth9603 3 года назад +1

    Looks like there was too much boost and too little fuel and the ignition was too high to me but it might be worth investing in some forged pistons when rebuilding the engine

  • @IsaacArnall
    @IsaacArnall 3 года назад

    Great video Steve 👌👍

  • @ianc427
    @ianc427 3 года назад

    I changed a turbo on my driveway with a friend easy good cars to take apart and rebuild

  • @2strokemxclassics
    @2strokemxclassics 3 года назад

    Nice one m8 been looking forward to this 👍

  • @oddssey2005
    @oddssey2005 3 года назад +3

    Maybe on the new engine run a different type of coolant and run your fan on when you are on track.
    I also think you need to port your engine it will help with the engine gases.good video best of lucky

    • @mrmarku
      @mrmarku 3 года назад

      John Deere cool gard, they run it mini migilia race cars.

  • @Pwilliamz
    @Pwilliamz 3 года назад +2

    great vid steve, dont think the wifes going to be too happy about the bedding tho lol

  • @Cars2Travel
    @Cars2Travel 3 года назад

    Great content keep it coming 👍

  • @citymotorfabuk
    @citymotorfabuk 3 года назад

    Well just what i said and was one of the first give my self pat on back cheers Steve

  • @F34rwaffles
    @F34rwaffles 3 года назад +2

    yup, I called it lol melted a hole in it, not the first time that's happened on this engine. I sent you the Ford 1.6 Ecoboost repair manual, give her a look, it might help you stumble through like it has me

  • @jeremyknight8569
    @jeremyknight8569 3 года назад

    Steve, Ford didn't bring the sleeve all the way to the top of the block. It ends just below the Head mating surface. that coolant passage between the cylinders makes for a thin spot that flexes and deforms under heat and stress. You said in the video that there was a little bit of movement right where cylinder 1 and 2 meet. This is a common problem. You can get the Mountune supported block or you can look at a couple of other options who are re-sleeving the block completely. That is probably why there was a clean spot above the failed area on piston one.
    J

  • @kevinpratt8122
    @kevinpratt8122 3 года назад

    Not enough fuel on map, That engine is not a loss steve plus would make good content rebuilding it

  • @christopherwoodhead7021
    @christopherwoodhead7021 3 года назад +15

    Ring gap was to small like I said in your last video.
    Rings expanded to much created to much heat up and down the bore.

    • @kd2833
      @kd2833 2 года назад

      What can prevent that ?

    • @kd2833
      @kd2833 2 года назад

      Yo

    • @romanr4409
      @romanr4409 2 года назад

      @@kd2833 what can prevent that? Either better cooling ( which night not help ya with too much boost ) or file down the ring gap. In burgerland engines get granaded all the time because of 200 shot leans the engine out gets real hot closes the gap and breaks the piston.

  • @JobForACowboy0069
    @JobForACowboy0069 3 года назад

    Is the block really that bad, have you got a straight edge and feeler guage to check it's not warped. Just thinking you could have that bore decked and stick a new piston in

  • @PaulL42654
    @PaulL42654 3 года назад +3

    "it's quite dramatic when an engine blows", just shows how amazing modern engineering is!
    is a forged one going in?

  • @Ktmandsuzuki
    @Ktmandsuzuki 3 года назад +1

    Dont know much about those engines but id say the extra power was just a bit too much for that piston probably not helped by too much heat.
    Hope you get it sorted and it doesnt cost you too much money.

  • @paulthompson5416
    @paulthompson5416 3 года назад +4

    Steve I’m almost certain yobo only needed an oil change to get rid of the little chunks of joy 🤷🏼‍♂️🥴

  • @opexo
    @opexo 3 года назад

    in my opinion for some reason №1 leaned out and started to melt, then as soon as the material got softer the high pressure of the combustion blew past the top of the piston and broke it down. Good that you reacted fast and stopped pushing otherwise it could be a catastrofic faiIure with hole on the block etc and everything mangled. I still think this power level is the top the engine can handle in standard form and i still think new sleeves and pistons can be put in it which would open it up for more power while safe at the same time. But who knows what's ur next plans, maybe something even better :)

  • @DAVESDIYDEN
    @DAVESDIYDEN 3 года назад

    Very unfortunate Steve. Im no mechanic but looking at the piston I would say there has been a hotspot within the combustion chamber perhaps because of a blockage in the cooling channel. causing uneven cooling. maybe why the other chamber has a crack in it it too? insufficient or old coolant over winter causing freezing and expansion? just some thoughts

  • @samcook7046
    @samcook7046 3 года назад

    At least your turbo is okay. This is most likely down to the tune you think? I’ve heard about a few fiestas up to 350hp on a stock engine being fine for years.

  • @therat5680
    @therat5680 3 года назад

    Nice work 👍

  • @iainnewton1674
    @iainnewton1674 3 года назад +7

    Should make it into a coffee table 😂😂😂

  • @dannycurtis1744
    @dannycurtis1744 3 года назад

    Could be a couple of things ,it could have started with a crack in that piston then the broke up under load, or just started with a broken ring. You need the other 3 out to compare 👍

  • @Logicalx
    @Logicalx 3 года назад

    Not a mechanic, though I have interests like you Steve and do a lot of stuff on my car myself. But, for this failure. Is it possible that the map has something to do with it? Which made the injector spaz out and in turn made it run lean and cause the piston to melt?

  • @jakeedwards5332
    @jakeedwards5332 3 года назад

    Could make a Nice engine block coffee table now 😂

  • @flippingcarsrepairs
    @flippingcarsrepairs 3 года назад

    That was a brave move using the joists on the roof 😮😮😮

    • @Sparkplugsteve
      @Sparkplugsteve 3 года назад

      I built the roof so know its capabilities 😂

  • @dixiedean2911
    @dixiedean2911 3 года назад

    Epic video Steve, not an expert either I agree with you it doesn't look good 😉
    The big question I have is what are you replacing it with......😜👍

  • @Rust_valley_racing
    @Rust_valley_racing 3 года назад

    Heads off it so it be worth getting it gas flowed and open up the ports ?? Or even practice on a die grinder and open the ports up ??