Vince Hogg
Vince Hogg
  • Видео 73
  • Просмотров 100 896
Back to non FPV firmware
The previous video was using the FPV firmware. The jumps/jitters were huge and violent. Went back to non FPV firmware for this vid. Starts off with a bad loss of level, then back to the less severe (but unacceptable ) jitters. It seems to be ok if the pitch is level. Im wondering if its a hardware problem with the gimbal. (the pitch changes in the first few seconds are me. )
Просмотров: 59

Видео

HEQ gport Gimbal Jumping. FPV firmware.
Просмотров 742 месяца назад
Just updated the firmware to VER-1000019 (file FPVmode-Firmware-APP_V1.0.0.25_20240509). As you see, there is terrible jumping around. To prove its not my RC TX outputting bad signals I set ardupilot to output fixed PWM on yaw and pitch. Notice that sometimes 2 axis jump together, not just pitch. Not shown in this clip but there was bad horizon drift. FPV mode works as it should and locks the g...
First test of HEQ gport gimbal on plane.
Просмотров 1162 месяца назад
Gimbal is installed on a retractable mount. Im using sbus to control yaw and pitch. There is some jittering in the gimbal axis, particularly when its not facing straight forward. Also as you see, it seems to loose which way is up and the horizon has a considerable tilt. HEQ support are very responsive and suggest the jittering is interference in the lines. (EDIT The twitching could be originati...
HEQ gport gimbal twitch when using sbus
Просмотров 642 месяца назад
Gimbal often twitches at all pitch angles but is much worse at about 45deg down. It does not do this twitch when using PWM. It also has quite a bit of roll drift. (Horizon not level).
HEQ gport gimbal sbus home not working
Просмотров 1752 месяца назад
Really like the hardware of this gimbal. Just needs a few tweaks of the firmware and it will be great. Note that the FPV version of the firmware locks at least one axis. It can’t be selected from RC (currently).
Gimbal retract tested on Goose plane.
Просмотров 1023 месяца назад
Gimbal retract tested on Goose plane.
HEQ g-port gimbal retract unit.
Просмотров 4523 месяца назад
Gimbal retract unit for HEQ g-port
4 May 2024
Просмотров 744 месяца назад
CRSF losing bind. Need this process to reconnect.
Lidl Glider drop
Просмотров 2395 месяцев назад
Lidl Glider drop
7 March 2024
Просмотров 256 месяцев назад
CRSF settings.
Problems with CRSF - FC connection
Просмотров 506 месяцев назад
Continuing problems with TBS CRSF - FC connection. Sometimes the RX looses bind. Today bind seems ok with 100% LQ but FC not seeing RC. Often loosing bind in flight.
Last day as commercial pilot.
Просмотров 1,5 тыс.6 месяцев назад
Last day as commercial pilot.
Tough test for Ardurover.
Просмотров 71410 месяцев назад
Tough test for Ardurover.
Ardurover testing with Herelink. RC Crawler.
Просмотров 4,1 тыс.10 месяцев назад
Ardurover testing with Herelink. RC Crawler.
Rover vehicle rough ground test. Ardurover on Pixhawk cube & Herelink.
Просмотров 1,3 тыс.Год назад
Rover vehicle rough ground test. Ardurover on Pixhawk cube & Herelink.
Solidworks Shell feature issues. Workaround tutorial.
Просмотров 4,8 тыс.3 года назад
Solidworks Shell feature issues. Workaround tutorial.
FX Wildcat 8 shot magazine quick loader - 177.
Просмотров 3,6 тыс.4 года назад
FX Wildcat 8 shot magazine quick loader - 177.
Effect of scope cant - some theory
Просмотров 1714 года назад
Effect of scope cant - some theory
AA S410 22 barrel bent where necked down for moderator.
Просмотров 1194 года назад
AA S410 22 barrel bent where necked down for moderator.
Drone IR camera stability issue.
Просмотров 2094 года назад
Drone IR camera stability issue.
Solex on Herelink gimbal control issue.
Просмотров 1,1 тыс.4 года назад
Solex on Herelink gimbal control issue.
Testing Runcam NightEagle 2pro as handheld spotter.
Просмотров 1924 года назад
Testing Runcam NightEagle 2pro as handheld spotter.
Vision 750 review and faults.
Просмотров 2314 года назад
Vision 750 review and faults.
DIY night vision
Просмотров 1734 года назад
DIY night vision
Fallow deer near Benington
Просмотров 1264 года назад
Fallow deer near Benington
Funchal Madeira approach training in A320 simulator.
Просмотров 1064 года назад
Funchal Madeira approach training in A320 simulator.
Drone Gimbal Vibration Testing
Просмотров 2,1 тыс.4 года назад
Drone Gimbal Vibration Testing
Printed modification to Autel EVO controller to take an ipad or other large tablet.
Просмотров 1614 года назад
Printed modification to Autel EVO controller to take an ipad or other large tablet.
Herelink gimbal setup
Просмотров 8 тыс.5 лет назад
Herelink gimbal setup
Test With Herelink And Camera
Просмотров 1 тыс.5 лет назад
Test With Herelink And Camera

Комментарии

  • @hiddeye
    @hiddeye День назад

    Hello, what is your frame ? please

  • @Magneticitist
    @Magneticitist 2 месяца назад

    I don't have any jitter on the pitch normally but the Yaw goes nuts when locking it with the new firmware. That's using an RC truck though. I think the jitter still comes through sometimes without locking it but just not as much. The only time I actually saw my pitch jitter was when I transmitted to a baofeng radio I put on the truck. While you may not be putting out bad signals, it's apparently not very noise immune since just the amp on the baofeng doing receiving is wigging mine out.

  • @sergiooropeza5602
    @sergiooropeza5602 2 месяца назад

    Mine does the same... did you find any solution?, i also try by pwm and its the same

    • @vincehogg8935
      @vincehogg8935 2 месяца назад

      Didnt have time to work on it for a while. Someone said the 'new' firmware is better. Im not sure which one he meant. The only new one I see (from yesterday) is for mavlink. I would like to use that but there is no information how to set it up. ie which gimbal to select in Mission Planner etc.

    • @sergiooropeza5602
      @sergiooropeza5602 2 месяца назад

      @@vincehogg8935 that firmware that includes mavlink may work better but I can see that for using with ardupilot you need to compile it, since the include the source code for driving the the gimbal by mavlink commands

    • @vincehogg8935
      @vincehogg8935 2 месяца назад

      Tested today with the FPV firmware. Very bad gimbal jumping. See my vid loaded today. Im wondering if I have a faulty gimbal. I tried pulling off my sbus wire and the gimbal just stays at its last setting. It dosent jump around.

    • @vincehogg8935
      @vincehogg8935 2 месяца назад

      All my tests have been in angle mode. I tried speed mode on sbus and it behaves like the 'home' is randomly applied. I then tried speed mode with PWM connections and it seems fine (with FPV firmware 000019). So only one way working. PWM speed mode.

  • @HEQUAV
    @HEQUAV 2 месяца назад

    Cool!

  • @sergiooropeza5602
    @sergiooropeza5602 2 месяца назад

    Did you try to offset the pwm signal?, i mean... trying diferent pwm values? i guess the pw pass from free to home lock and then free again...

  • @charleyboy74
    @charleyboy74 2 месяца назад

    Pretty cool, used similar motors myself.

  • @pachanoid
    @pachanoid 2 месяца назад

    muy bueno algo asi es lo que necesito

  • @kaspersorensen
    @kaspersorensen 3 месяца назад

    Nice! I get your thinking. HEQ should consider designing a gimbal which is better suited for upward mounting, or extend the negative pitch

  • @Crunklefloop
    @Crunklefloop 3 месяца назад

    Are you just having issues on the bench when plugged in on USB? There have been some reports of issues with the Matek USB board (the external board). I get an intermittent issue with my crossfire where it suddenly locks up on the bench. Absolutely fine in flight though.

  • @sergiooropeza5602
    @sergiooropeza5602 3 месяца назад

    Great Vince!!!

  • @Crunklefloop
    @Crunklefloop 3 месяца назад

    Jist make sure that in the event of RX failsafe it is set to retract before the Autoland.

    • @vincehogg8935
      @vincehogg8935 3 месяца назад

      Yes exactly. I thought I found the setting to make sure that happened but now have lost it.

  • @sergiooropeza5602
    @sergiooropeza5602 3 месяца назад

    Hey!!! you made it! i'm following your ptoject on Ardupilot Forum!, how much does it weight? only the retract sys?

    • @vincehogg8935
      @vincehogg8935 3 месяца назад

      I think it’s about the same weight as the gimbal, 70g. I think there may be a better (lighter) servo option, slow but high torque. Guess I need to buy the gimbal now.

    • @sergiooropeza5602
      @sergiooropeza5602 3 месяца назад

      @@vincehogg8935 Looks really functional, i'm about to buy the gimbal too.... could you share your files?

    • @vincehogg8935
      @vincehogg8935 3 месяца назад

      @@sergiooropeza5602 Ok I’ll put them on grabcad tomorrow probably.

    • @sergiooropeza5602
      @sergiooropeza5602 3 месяца назад

      @@vincehogg8935 Great! Thks!!!

  • @TheLastRealPanda
    @TheLastRealPanda 3 месяца назад

    put soft-ish springs underneath the carrier, on the rails

  • @jasonstation
    @jasonstation 3 месяца назад

    My issues are intermittent - my last two flights - absolutely nothing happened. So grateful this all started happening while operating something capable of landing itself.

  • @terrylembke8100
    @terrylembke8100 4 месяца назад

    that is an awesome build . I am starting to do some robotic builds myself . I am retired and learning a lot of new things . keeping my brain active and having fun . thank you for sharing look forward to seeing more of your projects .

  • @VolodymyrFedoschuk
    @VolodymyrFedoschuk 4 месяца назад

    What are the advantages of such horizontal suspension?

    • @vincehogg8935
      @vincehogg8935 4 месяца назад

      None. Thats why I changed it.

  • @aya-allahmedhat5235
    @aya-allahmedhat5235 4 месяца назад

    شكرا جدا ليك

  • @geofrancis2001
    @geofrancis2001 5 месяцев назад

    I like the chassis.

  • @aptech2933
    @aptech2933 5 месяцев назад

    That thing's awesome!

  • @RajKumar-kn9xe
    @RajKumar-kn9xe 5 месяцев назад

    Wonderfull work. 🙌🙌🙌

  • @user-gl4yh6fe6e
    @user-gl4yh6fe6e 5 месяцев назад

    ?????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????????

  • @miawoodward8028
    @miawoodward8028 6 месяцев назад

    Love you man

  • @DiMonteGroup
    @DiMonteGroup 8 месяцев назад

    Vince - great job on this! I've been an an advocate of "Split Part shell" for about 15 years. For what it is worth, you did not need to make a surface - you could just use Sketch 3 for the split. It's just a minor tweak, the general approach is solid. I use it all the time

  • @cristiansandor4435
    @cristiansandor4435 Год назад

    Great solution! Thanks for sharing.

  • @DIYGuy85
    @DIYGuy85 Год назад

    Max power of 1kw meaning it has 250watt motor x 4?

  • @dynamixsystems
    @dynamixsystems Год назад

    I design 3D Printed UAVs and had the same issue around the edges. thank you very much!

  • @jasona.neverforgetfukushim647

    What keeps the pellets from dropping out? An elastic band? O-ring? Does it work with slugs? Nice design though! Thanks for sharing. Cheers!

  • @79ober
    @79ober Год назад

    nice!

  • @teamfugldriverpops7850
    @teamfugldriverpops7850 Год назад

    Are you going to try selling this

  • @RizHassan
    @RizHassan 2 года назад

    Hi Vince, were you able to 3d print the aircraft? I am finding that Cura cannot print parts with shell and solid features. A part has to be either a solid extrusion or a shell, cannot be both.

    • @vincehogg8935
      @vincehogg8935 2 года назад

      Hi, yes I have printed the aircraft with few problems. I use S3D on homemade printer. However since then I have had big work changes and have not had enough time to finish it.

  • @akivaweil5066
    @akivaweil5066 2 года назад

    This was surprisingly interesting. Thanks for sharing

  • @houseofbrokendobbsthings5537
    @houseofbrokendobbsthings5537 2 года назад

    Very detailed - thank you for sharing.

  • @davisdesigns1153
    @davisdesigns1153 2 года назад

    Thank you!!! You've saved my ass, I've been struggling for hours

  • @eded9208
    @eded9208 2 года назад

    Brilliant, you have saved me from hours of torment...lol. Great workaround thank you.

  • @davisw13
    @davisw13 2 года назад

    How did this payload work out? I'd love to see the video feed.

  • @brezovprut4431
    @brezovprut4431 2 года назад

    This is C mount lens converted to M12 screw ?

  • @palletface2
    @palletface2 2 года назад

    Hey Vince, was looking for a workaround to a similar problem and couldn’t find a solution that didn’t entail changing the external geometry. Something my customer couldn’t consider. Great method, thank you. Would be interested to see more of your projects.

    • @vincehogg8935
      @vincehogg8935 2 года назад

      Thanks for that. Not many projects at the moment, apart from house fixing.

  • @airfilm_it
    @airfilm_it 2 года назад

    can the herelink be used as standalone video tx-rx?

  • @jeneilpringle215
    @jeneilpringle215 2 года назад

    Hows this project coming along?

  • @hardin1306
    @hardin1306 2 года назад

    Which gimbal is this

  • @DemiFlower1010
    @DemiFlower1010 2 года назад

    hi could you answer a couple questios please? how did you wire your gimbal and what settings did you set on the herelink i can not get mine going if you would like myn email mioght be easier thanks

  • @sibujacob977
    @sibujacob977 2 года назад

    Can you advice where i could locate a power cable connector for the Airlink of the Herelink

  • @markc3571
    @markc3571 2 года назад

    Too bad you can’t just pour the pellets in the top of the chamber and shake it and have them drop down inside your loading chamber to make it easier, instead of loading them by hand into your chamber. But great idea nevertheless.

  • @misterpotato2
    @misterpotato2 3 года назад

    Thanks for the video. I reached to your video after i have problem to control camera gimbal. As nowadays there are lot of camera gimbal with integrated camera, and it seems herelink is not very well with them. What i actually means is that, 1. Herelink only provide 1 very small hardware wheel in which it can be use to give pwm value to any movement that you would made. But it is self centered, in which will cause headache for pitch gimbal control. Obviously you need two wheel, 1 for pitch and 1 other for yaw. They should do update. (I ordered the herelink from foxtech and it do arrive yesterday). 2. And as the gimbal is now have more functions like yours, digital zoom, rec, stop rec, the button itself cannot control these camera although through pixhawk cube. Here i can see need to have seagull rec for this purposes. More headache. 3. Two sbus cable on the air unit but only one can be use. What is this another cable use for? If only you guys can reply my comments, and give answers, i would definitely like to hear it. If no answers, then keep away from herelink remote controller although they are advertised with pixhawk cube.

  • @ravisingh7329
    @ravisingh7329 3 года назад

    Hey How did you get to show soo many channels on your buttons tab of QGC. I can only see 4 or 5 channels on mine.

  • @theunknown964
    @theunknown964 3 года назад

    Hi. I will be using solex as my default app. This is my solex settings along with my pixhawk cube orange pins for which I have connected a three axis gimbal. In solex, (I have set the wheel settings by default to RC CH : 9 and I have connected the pitch axis of my gimbal to AUXILIARY : 1 of my pixhawk cube orange pin) and (I have assigned A short press to change the wheel settings to CH : 10 and I have connected the yaw axis of my gimbal to AUXILIARY : 2 of my pixhawk cube orange pin) and (A long press is assigned as clear wheel settings to get back to CH : 9) This all are done in solex tx app in herelink. And another thing is that A short press and A long press, both the button channels are set in as toggle button and not a momentary button in herelink original settings, so will the above setup for gimbal work as I expect ? Should I set to toggle or momentary for the A short press and A long press ?

  • @theunknown964
    @theunknown964 3 года назад

    Hi. I will be using solex as my default app. This is my solex settings along with my pixhawk cube orange pins for which I have connected a three axis gimbal. In solex, (I have set the wheel settings by default to RC CH : 9 and I have connected the pitch axis of my gimbal to AUXILIARY : 1 of my pixhawk cube orange pin) and (I have assigned A short press to change the wheel settings to CH : 10 and I have connected the yaw axis of my gimbal to AUXILIARY : 2 of my pixhawk cube orange pin) and (A long press is assigned as clear wheel settings to get back to CH : 9) This all are done in solex tx app in herelink. And another thing is that A short press and A long press, both the button channels are set in as toggle button and not a momentary button in herelink original settings, so will the above setup for gimbal work as I expect ? Should I set to toggle or momentary for the A short press and A long press ?

  • @theunknown964
    @theunknown964 3 года назад

    Hi. I will be using solex as my default app. This is my solex settings along with my pixhawk cube orange pins for which I have connected a three axis gimbal. In solex, (I have set the wheel settings by default to RC CH : 9 and I have connected the pitch axis of my gimbal to AUXILIARY : 1 of my pixhawk cube orange pin) and (I have assigned A short press to change the wheel settings to CH : 10 and I have connected the yaw axis of my gimbal to AUXILIARY : 2 of my pixhawk cube orange pin) and (A long press is assigned as clear wheel settings to get back to CH : 9) This all are done in solex tx app in herelink. And another thing is that A short press and A long press, both the button channels are set in as toggle button and not a momentary button in herelink original settings, so will the above setup for gimbal work as I expect ? Should I set to toggle or momentary for the A short press and A long press ?

  • @theunknown964
    @theunknown964 3 года назад

    Hi. I will be using solex as my default app. This is my solex settings along with my pixhawk cube orange pins for which I have connected a three axis gimbal. In solex, (I have set the wheel settings by default to RC CH : 9 and I have connected the pitch axis of my gimbal to AUXILIARY : 1 of my pixhawk cube orange pin) and (I have assigned A short press to change the wheel settings to CH : 10 and I have connected the yaw axis of my gimbal to AUXILIARY : 2 of my pixhawk cube orange pin) and (A long press is assigned as clear wheel settings to get back to CH : 9) This all are done in solex tx app in herelink. And another thing is that A short press and A long press, both the button channels are set in as toggle button and not a momentary button in herelink original settings, so will the above setup for gimbal work as I expect ? Should I set to toggle or momentary for the A short press and A long press ?

  • @theunknown964
    @theunknown964 3 года назад

    Hi. I will be using solex as my default app. This is my solex settings along with my pixhawk cube orange pins for which I have connected a three axis gimbal. In solex, (I have set the wheel settings by default to RC CH : 9 and I have connected the pitch axis of my gimbal to AUXILIARY : 1 of my pixhawk cube orange pin) and (I have assigned A short press to change the wheel settings to CH : 10 and I have connected the yaw axis of my gimbal to AUXILIARY : 2 of my pixhawk cube orange pin) and (A long press is assigned as clear wheel settings to get back to CH : 9) This all are done in solex tx app in herelink. And another thing is that A short press and A long press, both the button channels are set in as toggle button and not a momentary button in herelink original settings, so will the above setup for gimbal work as I expect ? Should I set to toggle or momentary for the A short press and A long press ?